Refactor the output report sending functions to allow for the sending of output
reports without enqueuing a work item. Output reports for any device can now be
sent via the send_output_report function pointer in the sony_sc struct which
points to the appropriate output function. The individual state worker
functions have been replaced with a universal sony_state_worker function which
uses this function pointer.
Signed-off-by: Frank Praznik <frank.praznik@gmail.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
When configuring input device via input_configured callback we may
encounter errors (for example input_mt_init_slots() may fail). Instead
of continuing with half-initialized input device let's allow driver
indicate failures.
Signed-off-by: Jaikumar Ganesh <jaikumarg@android.com>
Signed-off-by: Arve Hjønnevåg <arve@android.com>
Reviewed-by: Benjamin Tissoires <benjamin.tissoires@redhat.com>
Reviewed-by: David Herrmann <dh.herrmann@gmail.com>
Acked-by: Nikolai Kondrashov <Nikolai.Kondrashov@redhat.com>
Acked-by: Andrew Duggan <aduggan@synaptics.com>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
This commit removes the cap on the DualShock 4 controller reporting rate when
connected using Bluetooth. The previous value of '0xB0' capped the rate to only
20.83 Hz which many userspace utilities mistook as a sign of a bad signal.
Since a 'B' and an '8' can look similar it's possible that someone mistook the
one for another. The new value of '0x80' enables the full 1000 Hz peak
reporting rate that the controller is capable of.
Frank adds: "Back when the original code was written the purpose of that value
was unknown and 0xB0 seemed to work so that's what ended up being used. Now
that we know what it actually does and that 0x80 is a better choice I support
this patch."
[jkosina@suse.com: update changelog]
Signed-off-by: Rostislav Pehlivanov <atomnuker@gmail.com>
Acked-by: Frank Praznik <frank.praznik@gmail.com>
Signed-off-by: Jiri Kosina <jkosina@suse.com>
When connected via Bluetooth the sixaxis periodically sends reports with an ID
of 1, the second byte 0xff and the rest zeroed. These reports are not related
to the controller state and must be dropped to avoid generating false input
events.
Link: http://www.spinics.net/lists/linux-bluetooth/msg63028.html
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.com>
Fix the report descriptor so that the buttons and trigger are correctly reported.
The format of the input report is described here:
https://github.com/nitsch/moveonpc/wiki/Input-report
The Accelerometers and Gyros (1st frame only) are also reported as axis, but
the Magnetometers are NOT as 'fixing' their byte order would break user-space
drivers such as PSMoveAPI.
It is hoped to resolve this at a future time.
Signed-off-by: Simon Wood <simon@mungewell.org>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
The LED and Rumble control only function via BT if the full output report
is sent. The large report still functions via USB.
Signed-off-by: Simon Wood <simon@mungewell.org>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Add support for the battery charge level and state to be read via BT.
This is not support via USB as there is no know way to get the device
sending 'input' reports over USB.
Signed-off-by: Simon Wood <simon@mungewell.org>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Split quirk for PS Move Controller as it has to be treated differently
when connected via BT.
Signed-off-by: Simon Wood <simon@mungewell.org>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Correct a spelling mistake in the Sixaxis HID descriptor comment.
Add an explanation as to why the Sixaxis has so many analog axes and why
some of them are seen as multi-touch axes.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Acked-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Directly set the initial LED states in the device state struct instead
of copying them from a temporary array.
This allows for the removal of a redundant "x = x" copy loop in
sony_set_leds() that was taking place any time an LED was updated.
It also allows for the simplifying of the parameters in functions dealing
with LED initialization and updates since only a pointer to the sony_sc
struct is needed now.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Acked-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Add a fixed-up HID descriptor for the Sony motion controller and enable
controls for the LED light as well as force-feedback.
The LED is multi-colored (red, green, blue).
The motion controller has a single rumble motor so the higher of the left
and right values is used to set the speed.
Signed-off-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Acked-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
sony_allocate_output_report() was being called before sony_set_device_id()
which meant that an unallocated ida value was was freed if the output
report allocation failed and the probe function jumped to err_stop.
Do the device ID allocation before the output report allocation to avoid
freeing an unallocated value in case of a failure.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Acked-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Pull HID updates from Jiri Kosina:
- quite a few firmware fixes for RMI driver by Andrew Duggan
- huion and uclogic drivers have been substantially overlaping in
functionality laterly. This redundancy is fixed by hid-huion driver
being merged into hid-uclogic; work done by Benjamin Tissoires and
Nikolai Kondrashov
- i2c-hid now supports ACPI GPIO interrupts; patch from Mika Westerberg
- Some of the quirks, that got separated into individual drivers, have
historically had EXPERT dependency. As HID subsystem matured (as
well as the individual drivers), this made less and less sense. This
dependency is now being removed by patch from Jean Delvare
- Logitech lg4ff driver received a couple of improvements for mode
switching, by Michal Malý
- multitouch driver now supports clickpads, patches by Benjamin
Tissoires and Seth Forshee
- hid-sensor framework received a substantial update; namely support
for Custom and Generic pages is being added; work done by Srinivas
Pandruvada
- wacom driver received substantial update; it now supports
i2c-conntected devices (Mika Westerberg), Bamboo PADs are now
properly supported (Benjamin Tissoires), much improved battery
reporting (Jason Gerecke) and pen proximity cleanups (Ping Cheng)
- small assorted fixes and device ID additions
* 'for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/jikos/hid: (68 commits)
HID: sensor: Update document for custom sensor
HID: sensor: Custom and Generic sensor support
HID: debug: fix error handling in hid_debug_events_read()
Input - mt: Fix input_mt_get_slot_by_key
HID: logitech-hidpp: fix error return code
HID: wacom: Add support for Cintiq 13HD Touch
HID: logitech-hidpp: add a module parameter to keep firmware gestures
HID: usbhid: yet another mouse with ALWAYS_POLL
HID: usbhid: more mice with ALWAYS_POLL
HID: wacom: set stylus_in_proximity before checking touch_down
HID: wacom: use wacom_wac_finger_count_touches to set touch_down
HID: wacom: remove hardcoded WACOM_QUIRK_MULTI_INPUT
HID: pidff: effect can't be NULL
HID: add quirk for PIXART OEM mouse used by HP
HID: add HP OEM mouse to quirk ALWAYS_POLL
HID: wacom: ask for a in-prox report when it was missed
HID: hid-sensor-hub: Fix sparse warning
HID: hid-sensor-hub: fix attribute read for logical usage id
HID: plantronics: fix Kconfig default
HID: pidff: support more than one concurrent effect
...
* new API for safe access of power supply function attrs
* devres support for power supply (un)registration
* new drivers / chips
- generic syscon based poweroff driver
- iio & charger driver for da9150
- fuel gauge driver for axp288
- bq27x00: add support for bq27510
- bq2415x: add support for bq24157s
* twl4030-madc-battery: convert to iio consumer
* misc fixes
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Merge tag 'for-v4.1' of git://git.infradead.org/battery-2.6
Pull power supply and reset changes from Sebastian Reichel:
- new API for safe access of power supply function attrs
- devres support for power supply (un)registration
- new drivers / chips:
- generic syscon based poweroff driver
- iio & charger driver for da9150
- fuel gauge driver for axp288
- bq27x00: add support for bq27510
- bq2415x: add support for bq24157s
- twl4030-madc-battery: convert to iio consumer
- misc fixes
* tag 'for-v4.1' of git://git.infradead.org/battery-2.6: (66 commits)
power: twl4030_madc_battery: Add missing MODULE_ALIAS
power: twl4030-madc-battery: Convert to iio consumer.
dt: power: Add docs for generic SYSCON poweroff driver.
power: reset: Add generic SYSCON register mapped poweroff.
power: max17042_battery: add missed blank
power: max17042_battery: Use reg type instead of chip type
power/reset: at91: big endian fixes for atsama5d3x
power_supply: charger-manager: Fix dereferencing of ERR_PTR
HID: input: Fix NULL pointer dereference when power_supply_register fails
power: constify of_device_id array
power/reset/rmobile-reset.c: Fix !HAS_IOMEM build
power_supply: 88pm860x_charger: Fix possible NULL pointer dereference and use of initialized variable
arm: mach-pxa: Decrement the power supply's device reference counter
mfd: ab8500: Decrement the power supply's device reference counter
power_supply: bq2415x_charger: Decrement the power supply's device reference counter
power_supply: 88pm860x_charger: Decrement the power supply's device reference counter
x86/olpc/xo15/sci: Use newly added power_supply_put API
x86/olpc/xo1/sci: Use newly added power_supply_put API
power_supply: charger-manager: Decrement the power supply's device reference counter
power_supply: Increment power supply use counter when obtaining references
...
Change the ownership of power_supply structure from each driver
implementing the class to the power supply core.
The patch changes power_supply_register() function thus all drivers
implementing power supply class are adjusted.
Each driver provides the implementation of power supply. However it
should not be the owner of power supply class instance because it is
exposed by core to other subsystems with power_supply_get_by_name().
These other subsystems have no knowledge when the driver will unregister
the power supply. This leads to several issues when driver is unbound -
mostly because user of power supply accesses freed memory.
Instead let the core own the instance of struct 'power_supply'. Other
users of this power supply will still access valid memory because it
will be freed when device reference count reaches 0. Currently this
means "it will leak" but power_supply_put() call in next patches will
solve it.
This solves invalid memory references in following race condition
scenario:
Thread 1: charger manager
Thread 2: power supply driver, used by charger manager
THREAD 1 (charger manager) THREAD 2 (power supply driver)
========================== ==============================
psy = power_supply_get_by_name()
Driver unbind, .remove
power_supply_unregister()
Device fully removed
psy->get_property()
The 'get_property' call is executed in invalid context because the driver was
unbound and struct 'power_supply' memory was freed.
This could be observed easily with charger manager driver (here compiled
with max17040 fuel gauge):
$ cat /sys/devices/virtual/power_supply/cm-battery/capacity &
$ echo "1-0036" > /sys/bus/i2c/drivers/max17040/unbind
[ 55.725123] Unable to handle kernel NULL pointer dereference at virtual address 00000000
[ 55.732584] pgd = d98d4000
[ 55.734060] [00000000] *pgd=5afa2831, *pte=00000000, *ppte=00000000
[ 55.740318] Internal error: Oops: 80000007 [#1] PREEMPT SMP ARM
[ 55.746210] Modules linked in:
[ 55.749259] CPU: 1 PID: 2936 Comm: cat Tainted: G W 3.19.0-rc1-next-20141226-00048-gf79f475f3c44-dirty #1496
[ 55.760190] Hardware name: SAMSUNG EXYNOS (Flattened Device Tree)
[ 55.766270] task: d9b76f00 ti: daf54000 task.ti: daf54000
[ 55.771647] PC is at 0x0
[ 55.774182] LR is at charger_get_property+0x2f4/0x36c
[ 55.779201] pc : [<00000000>] lr : [<c034b0b4>] psr: 60000013
[ 55.779201] sp : daf55e90 ip : 00000003 fp : 00000000
[ 55.790657] r10: 00000000 r9 : c06e2878 r8 : d9b26c68
[ 55.795865] r7 : dad81610 r6 : daec7410 r5 : daf55ebc r4 : 00000000
[ 55.802367] r3 : 00000000 r2 : daf55ebc r1 : 0000002a r0 : d9b26c68
[ 55.808879] Flags: nZCv IRQs on FIQs on Mode SVC_32 ISA ARM Segment user
[ 55.815994] Control: 10c5387d Table: 598d406a DAC: 00000015
[ 55.821723] Process cat (pid: 2936, stack limit = 0xdaf54210)
[ 55.827451] Stack: (0xdaf55e90 to 0xdaf56000)
[ 55.831795] 5e80: 60000013 c01459c4 0000002a c06f8ef8
[ 55.839956] 5ea0: db651000 c06f8ef8 daebac00 c04cb668 daebac08 c0346864 00000000 c01459c4
[ 55.848115] 5ec0: d99eaa80 c06f8ef8 00000fff 00001000 db651000 c027f25c c027f240 d99eaa80
[ 55.856274] 5ee0: d9a06c00 c0146218 daf55f18 00001000 d99eaa80 db4c18c0 00000001 00000001
[ 55.864468] 5f00: daf55f80 c0144c78 c0144c54 c0107f90 00015000 d99eaab0 00000000 00000000
[ 55.872603] 5f20: 000051c7 00000000 db4c18c0 c04a9370 00015000 00001000 daf55f80 00001000
[ 55.880763] 5f40: daf54000 00015000 00000000 c00e53dc db4c18c0 c00e548c 0000000d 00008124
[ 55.888937] 5f60: 00000001 00000000 00000000 db4c18c0 db4c18c0 00001000 00015000 c00e5550
[ 55.897099] 5f80: 00000000 00000000 00001000 00001000 00015000 00000003 00000003 c000f364
[ 55.905239] 5fa0: 00000000 c000f1a0 00001000 00015000 00000003 00015000 00001000 0001333c
[ 55.913399] 5fc0: 00001000 00015000 00000003 00000003 00000002 00000000 00000000 00000000
[ 55.921560] 5fe0: 7fffe000 be999850 0000a225 b6f3c19c 60000010 00000003 00000000 00000000
[ 55.929744] [<c034b0b4>] (charger_get_property) from [<c0346864>] (power_supply_show_property+0x48/0x20c)
[ 55.939286] [<c0346864>] (power_supply_show_property) from [<c027f25c>] (dev_attr_show+0x1c/0x48)
[ 55.948130] [<c027f25c>] (dev_attr_show) from [<c0146218>] (sysfs_kf_seq_show+0x84/0x104)
[ 55.956298] [<c0146218>] (sysfs_kf_seq_show) from [<c0144c78>] (kernfs_seq_show+0x24/0x28)
[ 55.964536] [<c0144c78>] (kernfs_seq_show) from [<c0107f90>] (seq_read+0x1b0/0x484)
[ 55.972172] [<c0107f90>] (seq_read) from [<c00e53dc>] (__vfs_read+0x18/0x4c)
[ 55.979188] [<c00e53dc>] (__vfs_read) from [<c00e548c>] (vfs_read+0x7c/0x100)
[ 55.986304] [<c00e548c>] (vfs_read) from [<c00e5550>] (SyS_read+0x40/0x8c)
[ 55.993164] [<c00e5550>] (SyS_read) from [<c000f1a0>] (ret_fast_syscall+0x0/0x48)
[ 56.000626] Code: bad PC value
[ 56.011652] ---[ end trace 7b64343fbdae8ef1 ]---
Signed-off-by: Krzysztof Kozlowski <k.kozlowski@samsung.com>
Reviewed-by: Bartlomiej Zolnierkiewicz <b.zolnierkie@samsung.com>
[for the nvec part]
Reviewed-by: Marc Dietrich <marvin24@gmx.de>
[for compal-laptop.c]
Acked-by: Darren Hart <dvhart@linux.intel.com>
[for the mfd part]
Acked-by: Lee Jones <lee.jones@linaro.org>
[for the hid part]
Acked-by: Jiri Kosina <jkosina@suse.cz>
[for the acpi part]
Acked-by: Rafael J. Wysocki <rafael.j.wysocki@intel.com>
Signed-off-by: Sebastian Reichel <sre@kernel.org>
Add new structure 'power_supply_config' for holding run-time
initialization data like of_node, supplies and private driver data.
The power_supply_register() function is changed so all power supply
drivers need updating.
When registering the power supply this new 'power_supply_config' should be
used instead of directly initializing 'struct power_supply'. This allows
changing the ownership of power_supply structure from driver to the
power supply core in next patches.
When a driver does not use of_node or supplies then it should use NULL
as config. If driver uses of_node or supplies then it should allocate
config on stack and initialize it with proper values.
Signed-off-by: Krzysztof Kozlowski <k.kozlowski@samsung.com>
Reviewed-by: Bartlomiej Zolnierkiewicz <b.zolnierkie@samsung.com>
Acked-by: Pavel Machek <pavel@ucw.cz>
[for the nvec part]
Reviewed-by: Marc Dietrich <marvin24@gmx.de>
[for drivers/platform/x86/compal-laptop.c]
Reviewed-by: Darren Hart <dvhart@linux.intel.com>
[for drivers/hid/*]
Reviewed-by: Jiri Kosina <jkosina@suse.cz>
Signed-off-by: Sebastian Reichel <sre@kernel.org>
Per-controller spinlock needs to be properly initialized during device probe.
[jkosina@suse.cz: massage changelog]
[jkosina@suse.cz: drop hunk that has already been applied by previous
patch]
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
sony_dev_list_lock spinlock (which was introduced in d2d782fcce ("HID: sony:
Prevent duplicate controller connections") is not being initialized properly.
Fix that.
Reported-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Don't mix declaration and allocation, remove some useless newlines
between calling a function and checking its return value.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Acked-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Use the same type declared in the prototypes of functions that are going
to accept the buffer as parameter.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Acked-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Remove the magic numbers used in sixaxis_set_operational_usb():
- use the already defined SIXAXIS_REPORT_0xF2_SIZE;
- define and use SIXAXIS_REPORT_0xF5_SIZE;
- set the dummy buffer size to accommodate any report that is going to
be requested.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Acked-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Sixaxis devices accept feature report 0xf2 when size is >= 17, not 18.
Use the minimum accepted size.
The change is mainly for documentation purposes, the code worked fine
even before this change.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Acked-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
ida_destroy() must be called _after_ all the devices have been
unregistered; otherwise, when calling "rmmod hid_sony" with devices
still plugged in, the following warning would show up because of calls
to ida_simple_remove() on a destroyed ID allocator:
------------[ cut here ]------------
WARNING: CPU: 0 PID: 5509 at lib/idr.c:1052 ida_simple_remove+0x26/0x50()
ida_remove called for id=0 which is not allocated.
Modules linked in: ...
CPU: 0 PID: 5509 Comm: rmmod Not tainted 3.19.0-rc6-ao2 #35
Hardware name: System manufacturer System Product Name/M2N-MX SE, BIOS 0501 03/20/2008
0000000000000000 ffffffff8176320d ffffffff815b3a88 ffff880036f7fdd8
ffffffff8106ce01 0000000000000000 ffffffffa07658e0 0000000000000246
ffff88005077d8b8 ffff88005077d8d0 ffffffff8106ce7a ffffffff81763260
Call Trace:
[<ffffffff815b3a88>] ? dump_stack+0x40/0x50
[<ffffffff8106ce01>] ? warn_slowpath_common+0x81/0xb0
[<ffffffff8106ce7a>] ? warn_slowpath_fmt+0x4a/0x50
[<ffffffff812ccb86>] ? ida_simple_remove+0x26/0x50
[<ffffffffa0762dc8>] ? sony_remove+0x58/0xe0 [hid_sony]
[<ffffffffa00fff15>] ? hid_device_remove+0x65/0xd0 [hid]
[<ffffffff8140425e>] ? __device_release_driver+0x7e/0x100
[<ffffffff81404c70>] ? driver_detach+0xa0/0xb0
[<ffffffff81403ee5>] ? bus_remove_driver+0x55/0xe0
[<ffffffffa01000ff>] ? hid_unregister_driver+0x2f/0xa0 [hid]
[<ffffffff810e45bf>] ? SyS_delete_module+0x1bf/0x270
[<ffffffff81014089>] ? do_notify_resume+0x69/0xa0
[<ffffffff815b952d>] ? system_call_fastpath+0x16/0x1b
---[ end trace bc794b3d22c30ede ]---
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Acked-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Without this, my "Gasia Co.,Ltd PS(R) Gamepad" would not send
any events. Now everything works including the leds.
Based on work by Andrew Haines and Antonio Ospite.
cc: Antonio Ospite <ao2@ao2.it>
cc: Andrew Haines <AndrewD207@aol.com>
Signed-off-by: Lauri Kasanen <cand@gmx.com>
Reviewed-by: Antonio Ospite <ao2@ao2.it>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Add vid/pid for the SMK branded third-party PS3 Bluetooth remote and enable
support in the hid-sony driver.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Replace stack buffers with kernel allocated buffers for sending
and receiving HID reports to prevent issues with DMA transfers
on certain hardware.
Output report buffers are allocated at initialization time to avoid
excessive calls to kmalloc and kfree.
Link: https://bugzilla.kernel.org/show_bug.cgi?id=87991
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Reviewed-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
The DualShock 4 touchpad has been measured to have a resolution of
44.86 dots/mm which equates to 1920x942.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Set the DualShock4 touchpad bits in the input_configured callback
so that they are registered properly for any input devices created
during hid_hw_start.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Update the file header and correct an outdated comment block.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Fix a few minor issues in the HID descriptor:
- A 6 bit entry had a logical maximum of 255 when the largest it can be is 63.
- A logical max value was incorrectly being set to -1 instead of 255.
- Set the min/max of the gyroscopes to -8192/8191 as that is the range of
values which represent the true controller orientation. Any values beyond
those extents are just noise.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Bit 3 in byte 31 of the Sixaxis report indicates whether the battery is
charging or not charging as opposed to whether or not the cable is plugged in.
As a result, when connected via USB and fully charged, the power_supply status
is wrongly reported as 'Discharging' instead of 'Full'.
Use the battery level value to set the cable state so that the power status
is reported correctly as that seems to be the only reliable way to determine the
cable status on the Sixaxis.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Previously only the first element of the array was initialized to 1
leading to potential incorrect max brightness values for the LEDs
on the Dualshock 3 and buzzer controllers.
Use a designated initializer to initialize the whole array to the
correct value.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Remove an old redundant comment before sony_report_fixup(), it must have
been a leftover from the first version of the driver:
sony_report_fixup() now handles all the supported devices, not only the
Sony Vaio VGX.
The comment is also redundant as the same information provided by it is
also present in the body of the function.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Reformat sixaxis_rdesc to reflect its HID structure, and comment each
field. This will make it easier to validate changes to the descriptor in
the future.
No functional changes are introduced, the descriptor is exactly the same
as before byte by byte.
The heavy lifting has been done with the help of hidrd-convert:
https://github.com/DIGImend/hidrd
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Simplify the logic of overriding the Sixaxis HID descriptor, this will
make it easier to amend the descriptor in future commits.
The current code does this:
if (original sixaxis via USB or BT)
fixup only a part of the descriptor
else if (sixaxis compatible controller)
override the _whole_ descriptor
but the end result is exactly the same, except for the trailing zero in
the case of original BT controllers.
So let's just regularize the process, and always override the HID
descriptor.
Always overriding the descriptor changes the current semantic a little
bit, before this change the BT descriptor still had the trailing zero
byte, while now it is exactly the same as the descriptor of the
controller via USB, but that does not affect proper operation of the
device.
Note that overriding the whole descriptor for original devices is not
strictly necessary for now, but it simplifies the code and in the future
the report descriptor will be patched further and keys will be remapped,
so it's handy to have only one place to patch.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Instead of checking for SIXAXIS_CONTROLLER_USB and SIXAXIS_CONTROLLER_BT
separately, a check on SIXAXIS_CONTROLLER can be used when setting
connect_mask.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Without this patch the 3rd party INTEC (PS3) controller will blink all
leds when user turns them off, it appears to require an extra flag set.
Signed-off-by: Simon Wood <simon@mungewell.org>
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Add support for setting the blink rate of the LEDs. The Sixaxis allows control
over each individual LED, but the Dualshock 4 only has one global control for
controlling the hardware blink rate so individual colors will fall back to
software timers.
Setting the brightness cancels the blinking as per the LED class specifications.
The Sixaxis and Dualshock 4 controllers accept delays in decisecond increments
from 0 to 255 (2550 milliseconds).
The value at index 1 of the DualShock 4 USB output report must be 0xFF or the
light bar won't blink.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Add an IDA id allocator to assign unique, sequential device ids to Sixaxis and
DualShock 4 controllers.
Use the device ID to initialize the Sixaxis and DualShock 4 controller LEDs to
default values. The number or color of the controller is set relative to other
connected Sony controllers.
Set the LED class brightness values to the initial values and add the new led to
the array before calling led_classdev_register so that the correct brightness
value shows up in the LED sysfs entry.
Use explicit module init and exit functions since the IDA allocator must be
manually destroyed when the module is unloaded.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Use the controller Bluetooth MAC address as the unique identifier in the
battery name string instead of the atomic integer that was used before.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Convert all of the local initialization and shutdown functions to take a
parameter type of struct sony_sc* instead of using a mix of struct sony_sc* and
struct hid_device*.
Allows for the removal of some calls to hid_get_drvdata().
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Use a struct for the Sixaxis output report that uses named members to set the
report fields.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Use inliners to make sure that the work queue initialization flag is always
checked and set correctly when initializing or cancelling the work queue.
Signed-off-by: Frank Praznik <frank.praznik@oh.rr.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>