This patch adds the required pieces to 8250-OMAP UART driver for DMA
support. The TX burst size is set to 1 so we can send an arbitrary
amount of bytes.
The RX burst is currently set to 48 which means we receive an DMA
interrupt every 48 bytes and have to reprogram everything. Less bytes in
the RX-FIFO mean that no DMA transfer will happen and the UART will send a
RX-timeout _or_ RDI event at which point the FIFO will be manually purged.
There is a workaround for TX-DMA on AM33xx where we put the first byte
into the FIFO to kick start the DMA process. Haven't seen this problem on
OMAP36xx (beagle board xm) or DRA7xx.
On AM375x there is "Usage Note 2.7: UART: Cannot Acknowledge Idle
Requests in Smartidle Mode When Configured for DMA Operations" in the
errata document. This problem persists even after disabling DMA in the
UART and will be addressed in the HWMOD.
v10:
- delay update_registers() from set_termios() until TX-DMA is
done. It has been reported / proved that invoking
update_registers() while TX-DMA is in progress may stall the
DMA operation and it won't finish.
- use the new omap DMA-TX-RX hooks and DMA only interrupt
routine.
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
We have (or will have) custom DMA callbacks in the omap driver due to
the different behaviour in the RX and TX case. To make this work
we need a few changes in the IRQ handler to invoke the rx_handler again
after the "manual" mode or retry the tx_handler again before falling
back to the manual mode.
Heikki didn't want to see the extra hacks in the generic / default irq
handler and Peter wasn't too happy about an OMAP-only IRQ handler. The
way I planned it is to use this extra IRQ routine only in DMA case. If
Peter dislike this approach then I hope Heikki doesn't block changes in
the default IRQ handler :)
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Heikki Krogerus <heikki.krogerus@linux.intel.com>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The omap needs a DMA request pending right away. If it is
enqueued once the bytes are in the FIFO then nothing will happen
and the FIFO will be later purged via RX-timeout interrupt.
This patch enqueues RX-DMA request on completion but not if it
was aborted on error. The first enqueue will happen in the driver
in startup.
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This patch provides mostly a copy of serial8250_tx_dma() +
__dma_tx_complete() with the following extensions:
- DMA bug
At least on AM335x the following problem exists: Even if the TX FIFO is
empty and a TX transfer is programmed (and started) the UART does not
trigger the DMA transfer.
After $TRESHOLD number of bytes have been written to the FIFO manually the
UART reevaluates the whole situation and decides that now there is enough
room in the FIFO and so the transfer begins.
This problem has not been seen on DRA7 or beagle board xm (OMAP3). I am not
sure if this is UART-IP core specific or DMA engine.
The workaround is to use a threshold of one byte, program the DMA
transfer minus one byte and then to put the first byte into the FIFO to
kick start the transfer.
- support for runtime PM
RPM is enabled on start_tx(). We can't disable RPM on DMA complete callback
because there is still data in the FIFO which is being sent. We have to wait
until the FIFO is empty before we disable it.
For this to happen we fake a TX sent error and enable THRI. Once the
FIFO is empty we receive an interrupt and since the TTY-buffer is still
empty we "put RPM" via __stop_tx(). Should it been filed then in the
start_tx() path we should program the DMA transfer and remove the error
flag and the THRI bit.
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The OMAP has a few corner cases where it needs a share of kindness of
affection to do the right thing. Heikki Krogerus suggested that instead
adding the quirks into the default DMA implementation, OMAP could get
its own copy of the function. And Alan suggested the same thing so here
we go.
This patch provides callbacks for custom TX/RX DMA implementation. If
there are not setup / used, then the default (current) implementation is
used.
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
After dmaengine_terminate_all() has been invoked then both DMA drivers
(edma and omap-dma) do not invoke dma_cookie_complete() to mark the
transfer as complete. This dma_cookie_complete() is performed by the
Synopsys DesignWare driver which is probably the only one that is used
by omap8250-dma and hence don't see following problem…
…which is that once a RX transfer has been terminated then following
query of channel status reports DMA_IN_PROGRESS (again: the actual
transfer has been canceled, there is nothing going on anymore).
This means that serial8250_rx_dma() never enqueues another DMA transfer
because it (wrongly) assumes that there is a transer already pending.
Vinod Koul refuses to accept a patch which adds this
dma_cookie_complete() to both drivers and so dmaengine_tx_status() would
report DMA_COMPLETE instead (and behave like the Synopsys DesignWare
driver already does). He argues that I am not allowed to use the cookie
to query the status and that the driver already cleaned everything up after
the invokation of dmaengine_terminate_all().
To end this I add a bookkeeping whether or not a RX-transfer has been
started to the 8250-dma code. It has already been done for the TX side.
*Now* we learn about the RX status based on our bookkeeping and don't
need dmaengine_tx_status() for this anymore.
Cc: vinod.koul@intel.com
Reviewed-by: Tony Lindgren <tony@atomide.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Right now it is possible that serial8250_tx_dma() fails and returns
-EBUSY. The caller (serial8250_start_tx()) will then enable
UART_IER_THRI which will generate an interrupt once the TX FIFO is
empty.
In serial8250_handle_irq() nothing will happen because up->dma is set
and so serial8250_tx_chars() won't be invoked. We end up with plenty of
interrupts and some "too much work for irq" output.
This patch introduces dma_tx_err in struct uart_8250_port to signal that
the last invocation of serial8250_tx_dma() failed so we can fill the TX
FIFO manually. Should the next invocation of serial8250_start_tx()
succeed then the dma_tx_err flag along with the THRI bit is removed and
DMA only usage may continue.
Reviewed-by: Tony Lindgren <tony@atomide.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This patch provides a 8250-core based UART driver for the internal OMAP
UART. The long term goal is to provide the same functionality as the
current OMAP uart driver and DMA support.
I tried to merge omap-serial code together with the 8250-core code.
There should should be hardly a noticable difference. The trigger levels
are different compared to omap-serial:
- omap serial
TX: Interrupt comes after TX FIFO has room for 16 bytes.
TX of 4096 bytes in one go results in 256 interrupts
RX: Interrupt comes after there is on byte in the FIFO.
RX of 4096 bytes results in 4096 interrupts.
- this driver
TX: Interrupt comes once the TX FIFO is empty.
TX of 4096 bytes results in 65 interrupts. That means there will
be gaps on the line while the driver reloads the FIFO.
RX: Interrupt comes once there are 48 bytes in the FIFO or less over
"longer" time frame. We have
1 / 11520 * 10^3 * 16 => 1.38… ms
1.38ms to react and purge the FIFO on 115200,8N1. Since the other
driver fired after each byte it had ~5.47ms time to react. This
_may_ cause problems if one relies on no missing bytes and has no
flow control. On the other hand we get only 85 interrupts for the
same amount of data.
It has been only tested as console UART on am335x-evm, dra7-evm and
beagle bone. I also did some longer raw-transfers to meassure the load.
The device name is ttyS based instead of ttyO. If a ttyO based node name
is required please ask udev for it. If both driver are activated (this
and omap-serial) then this serial driver will take control over the
device due to the link order
v9…v10:
- Tony noticed that omap3 won't show anything after waking up
from core off. In v9 I reworked the register restore and set
IER to 0 by accident. This went unnoticed because start_tx
usually sets ier (either due to DMA bug or due to TX-complete
IRQ).
- dropped EFR and SLEEP from capabilities. We do have both but
nobody should touch it. We already handle SLEEP ourself.
- make the private copy of the registers (like EFR) u8 instead
u32
- drop MDR1 & DL[ML] reset in restore registers. Does not look
required it is set to the required value later.
- update MDR1 & SCR only if changed.
- set MDR1 as the last thing. The errata says that we should
setup everything before MDR1 set.
- avoid div by 0 in omap_8250_get_divisor() if baud rate gets
very large (Frans Klaver fixed the same thing omap-serial)
- drop "is in early stage" from Kconfig.
v8…v9:
- less on a file seems to hang the am335x after a while. I
believe I introduce this bug a while ago since I can reproduce
this prior to v8. Fixed by redoing the omap8250_restore_regs()
v7…v8:
- redo the register write. There is now one function for that
which is used from set_termios() and runtime-resume.
- drop PORT_OMAP_16750 and move the setup to the omap file. We
have our own set termios function anyway (Heikki Krogerus)
- use MEM instead of MEM32. TRM of AM/DM37x says that 32bit
access on THR might result in data abort. We only need 32bit
access in the errata function which is before we use 8250's
read function so it doesn't matter.
v4…v7:
- change trigger levels after some tests with raw transfers.
v3…v4:
- drop RS485 support
- wire up ->throttle / ->unthrottle
v2…v3:
- wire up startup & shutdown for wakeup-irq handling.
- RS485 handling (well the core does).
v1…v2:
- added runtime PM. Could somebody could please double check
this?
- added omap_8250_set_termios()
Reviewed-by: Tony Lindgren <tony@atomide.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Tested-by: Frans Klaver <frans.klaver@xsens.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
if I boot with console=ttyS0 and the omap driver is module I end up with
| console [ttyS0] disabled
| omap8250 44e09000.serial: ttyS0 at MMIO 0x44e09000 (irq = 88, base_baud = 3000000) is a 8250
| Unable to handle kernel paging request at virtual address c07a9de0
| Modules linked in: 8250_omap(+)
| CPU: 0 PID: 908 Comm: modprobe Not tainted 3.17.0-rc5+ #1593
| PC is at serial8250_console_setup+0x0/0xc8
| LR is at register_console+0x13c/0x3a4
| [<c0078788>] (register_console) from [<c02d0340>] (uart_add_one_port+0x3cc/0x420)
| [<c02d0340>] (uart_add_one_port) from [<c02d38a4>] (serial8250_register_8250_port+0x298/0x39c)
| [<c02d38a4>] (serial8250_register_8250_port) from [<bf006274>] (omap8250_probe+0x218/0x3dc [8250_omap])
| [<bf006274>] (omap8250_probe [8250_omap]) from [<c02e3424>] (platform_drv_probe+0x2c/0x5c)
| [<c02e3424>] (platform_drv_probe) from [<c02e1eac>] (driver_probe_device+0x104/0x228)
…
| [<c009fa48>] (SyS_init_module) from [<c000e6e0>] (ret_fast_syscall+0x0/0x30)
| Code: 7823603b f8314620 051b3013 491ed416 (44792204)
because serial8250_console_setup() is already gone.
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Frans reworded the two comments with better English for better
understanding. His review hit the mailing list after the patch got
applied so here is an incremental update.
Reported-by: Frans Klaver <frans.klaver@xsens.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Added recognition of EndRun Technologies PCIe PTP slave card
and setup two ttySx ports for communication with the card for
retrieval of PTP based time and to communicate with the card's
Linux OS.
Signed-off-by: Mike Skoog <mskoog@endruntechnologies.com>
Signed-off-by: Mike Korreng <mkorreng@endruntechnologies.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In ST16650V2 based serial uarts, while initalizing the PM state,
LCR registers are being initialized to 0 in serial8250_set_sleep().
If console port is already initialized and being used, this will
throws garbage in the console.
Signed-off-by: Sudhir Sreedharan <ssreedharan@mvista.com>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Tested-by: Kevin Hilman <khilman@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Pull slave-dmaengine updates from Vinod Koul:
"For dmaengine contributions we have:
- designware cleanup by Andy
- my series moving device_control users to dmanegine_xxx APIs for
later removal of device_control API
- minor fixes spread over drivers mainly mv_xor, pl330, mmp, imx-sdma
etc"
* 'for-linus' of git://git.infradead.org/users/vkoul/slave-dma: (60 commits)
serial: atmel: add missing dmaengine header
dmaengine: remove FSLDMA_EXTERNAL_START
dmaengine: freescale: remove FSLDMA_EXTERNAL_START control method
carma-fpga: move to fsl_dma_external_start()
carma-fpga: use dmaengine_xxx() API
dmaengine: freescale: add and export fsl_dma_external_start()
dmaengine: add dmaengine_prep_dma_sg() helper
video: mx3fb: use dmaengine_terminate_all() API
serial: sh-sci: use dmaengine_terminate_all() API
net: ks8842: use dmaengine_terminate_all() API
mtd: sh_flctl: use dmaengine_terminate_all() API
mtd: fsmc_nand: use dmaengine_terminate_all() API
V4L2: mx3_camer: use dmaengine_pause() API
dmaengine: coh901318: use dmaengine_terminate_all() API
pata_arasan_cf: use dmaengine_terminate_all() API
dmaengine: edma: check for echan->edesc => NULL in edma_dma_pause()
dmaengine: dw: export probe()/remove() and Co to users
dmaengine: dw: enable and disable controller when needed
dmaengine: dw: always export dw_dma_{en,dis}able
dmaengine: dw: introduce dw_dma_on() helper
...
Here's the big tty/serial driver patchset for 3.18-rc1.
Lots of little things in here, some good work from Peter Hurley on the
tty core, and in lots of drivers. There are also lots of other driver
updates in here as well, full details in the changelog below.
All have been in the linux-next tree for a while.
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Merge tag 'tty-3.18-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty
Pull tty/serial driver updates from Greg KH:
"Here's the big tty/serial driver patchset for 3.18-rc1.
Lots of little things in here, some good work from Peter Hurley on the
tty core, and in lots of drivers. There are also lots of other driver
updates in here as well, full details in the changelogs.
All have been in the linux-next tree for a while"
* tag 'tty-3.18-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty: (99 commits)
Revert "serial/core: Initialize the console pm state"
tty: serial: 8250: use 32bit variable for rpm_tx_active
tty: serial: msm: Add earlycon support
serial/core: Initialize the console pm state
serial: asc: Conditionally use readl_relaxed (COMPILE_TEST)
serial: of-serial: add PM suspend/resume support
m68k: AMIGA_BUILTIN_SERIAL should depend on TTY
asm/uapi: Add definition of TIOC[SG]RS485
tty/metag_da: Add console_poll module parameter
serial: 8250_pci: remove rts_n override from Baytrail quirk
serial: cadence: Add generic earlycon support
serial: imx: change the wait even to interruptiable
serial: imx: terminate the RX DMA when the UART is suspending
serial: imx: fix throttle/unthrottle callbacks for hardware assisted flow control
serial: 8250: Add Quark X1000 to 8250_pci.c
tty: omap-serial: pull out calculation from baud_is_mode16
tty: omap-serial: fix division by zero
xen_hvc: no reason to write the type key on xenstore
tty: serial: 8250_core: remove UART_IER_RDI in serial8250_stop_rx()
tty: serial: 8250_core: use the ->line argument as a hint in serial8250_find_match_or_unused()
...
Cheers,
Rusty.
PS. My virtio-next tree is empty: DaveM took the patches I had. There might
be a virtio-rng starvation fix, but so far it's a bit voodoo so I will
get to that in the next two days or it will wait.
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Merge tag 'modules-next-for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/rusty/linux
Pull module update from Rusty Russell:
"Nothing major: support for compressing modules, and auto-tainting
params.
PS. My virtio-next tree is empty: DaveM took the patches I had. There
might be a virtio-rng starvation fix, but so far it's a bit voodoo
so I will get to that in the next two days or it will wait"
* tag 'modules-next-for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/rusty/linux:
moduleparam: Resolve missing-field-initializer warning
kbuild: handle module compression while running 'make modules_install'.
modinst: wrap long lines in order to enhance cmd_modules_install
modsign: lookup lines ending in .ko in .mod files
modpost: simplify file name generation of *.mod.c files
modpost: reduce visibility of symbols and constify r/o arrays
param: check for tainting before calling set op.
drm/i915: taint the kernel if unsafe module parameters are set
module: add module_param_unsafe and module_param_named_unsafe
module: make it possible to have unsafe, tainting module params
module: rename KERNEL_PARAM_FL_NOARG to avoid confusion
It should not be used together with Auto Flow Control, and
Auto Flow Control is always enabled on Baytrail.
Signed-off-by: Heikki Krogerus <heikki.krogerus@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Quark X1000 contains two designware derived 8250 serial ports.
Each port has a unique PCI configuration space consisting of
BAR0:UART BAR1:DMA respectively.
Unlike the standard 8250 the register width is 32 bits for RHR,IER etc
The Quark UART has a fundamental clock @ 44.2368 MHz allowing for a
bitrate of up to about 2.76 megabits per second.
This patch enables standard 8250 mode
Signed-off-by: Bryan O'Donoghue <pure.logic@nexus-software.ie>
Reviewed-by: Heikki Krogerus <heikki.krogerus@linux.intel.com>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
serial8250_do_startup() adds UART_IER_RDI and UART_IER_RLSI to ier.
serial8250_stop_rx() should remove both.
This is what the serial-omap driver has been doing and is now moved to
the 8250-core since it does no look to be *that* omap specific.
Reviewed-by: Heikki Krogerus <heikki.krogerus@linux.intel.com>
Reviewed-by: Tony Lindgren <tony@atomide.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Tony noticed that the old omap-serial driver picked the uart "number"
based on the hint given from device tree or platform device's id.
The 8250 based omap driver doesn't do this because the core code does
not honour the ->line argument which is passed by the driver.
This patch aims to keep the same behaviour as with omap-serial. The
function will first try to use the line suggested ->line argument and
then fallback to the old strategy in case the port is taken.
That means the the third uart will always be ttyS2 even if the previous
two have not been enabled in DT.
Reviewed-by: Tony Lindgren <tony@atomide.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The serial8250_do_startup() function unconditionally clears the
interrupts and for that it reads from the RX-FIFO without checking if
there is a byte in the FIFO or not. This works fine on OMAP4+ HW like
AM335x or DRA7.
OMAP3630 ES1.1 (which means probably all OMAP3 and earlier) does not like
this:
|Unhandled fault: external abort on non-linefetch (0x1028) at 0xfb020000
|Internal error: : 1028 [#1] ARM
|Modules linked in:
|CPU: 0 PID: 1 Comm: swapper Not tainted 3.16.0-00022-g7edcb57-dirty #1213
|task: de0572c0 ti: de058000 task.ti: de058000
|PC is at mem32_serial_in+0xc/0x1c
|LR is at serial8250_do_startup+0x220/0x85c
|Flags: nzCv IRQs on FIQs on Mode SVC_32 ISA ARM Segment kernel
|Control: 10c5387d Table: 80004019 DAC: 00000015
|[<c03051d4>] (mem32_serial_in) from [<c0307fe8>] (serial8250_do_startup+0x220/0x85c)
|[<c0307fe8>] (serial8250_do_startup) from [<c0309e00>] (omap_8250_startup+0x5c/0xe0)
|[<c0309e00>] (omap_8250_startup) from [<c030863c>] (serial8250_startup+0x18/0x2c)
|[<c030863c>] (serial8250_startup) from [<c030394c>] (uart_startup+0x78/0x1d8)
|[<c030394c>] (uart_startup) from [<c0304678>] (uart_open+0xe8/0x114)
|[<c0304678>] (uart_open) from [<c02e9e10>] (tty_open+0x1a8/0x5a4)
Reviewed-by: Tony Lindgren <tony@atomide.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
While comparing the OMAP-serial and the 8250 part of this I noticed that
the latter does not use run time-pm. Here are the pieces. It is
basically a get before first register access and a last_busy + put after
last access. This has to be enabled from userland _and_ UART_CAP_RPM is
required for this.
The runtime PM can usually work transparently in the background however
there is one exception to this: After serial8250_tx_chars() completes
there still may be unsent bytes in the FIFO (depending on CPU speed vs
baud rate + flow control). Even if the TTY-buffer is empty we do not
want RPM to disable the device because it won't send the remaining
bytes. Instead we leave serial8250_tx_chars() with RPM enabled and wait
for the FIFO empty interrupt. Once we enter serial8250_tx_chars() with
an empty buffer we know that the FIFO is empty and since we are not going
to send anything, we can disable the device.
That xchg() is to ensure that serial8250_tx_chars() can be called
multiple times and only the first invocation will actually invoke the
runtime PM function. So that the last invocation of __stop_tx() will
disable runtime pm.
NOTE: do not enable RPM on the device unless you know what you do! If
the device goes idle, it won't be woken up by incomming RX data _unless_
there is a wakeup irq configured which is usually the RX pin configure
for wakeup via the reset module. The RX activity will then wake up the
device from idle. However the first character is garbage and lost. The
following bytes will be received once the device is up in time. On the
beagle board xm (omap3) it takes approx 13ms from the first wakeup byte
until the first byte that is received properly if the device was in
core-off.
v5…v8:
- drop RPM from serial8250_set_mctrl() it will be used in
restore path which already has RPM active and holds
dev->power.lock
v4…v5:
- add a wrapper around rpm function and introduce UART_CAP_RPM
to ensure RPM put is invoked after the TX FIFO is empty.
v3…v4:
- added runtime to the console code
- removed device_may_wakeup() from serial8250_set_sleep()
Cc: mika.westerberg@linux.intel.com
Reviewed-by: Tony Lindgren <tony@atomide.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The OMAP UART provides support for HW assisted flow control. What is
missing is the support to throttle / unthrottle callbacks which are used
by the omap-serial driver at the moment.
This patch adds the callbacks. It should be safe to add them since they
are only invoked from the serial_core (uart_throttle()) if the feature
flags are set.
Reviewed-by: Tony Lindgren <tony@atomide.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add new PCI IDs to cover newer Intel SoCs such as Braswell.
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Mika Westerberg <mika.westerberg@linux.intel.com>
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Acked-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Signed-off-by: Vinod Koul <vinod.koul@intel.com>
That field has been deprecated in favour of getting the necessary information
from ACPI or DT.
However, we still need to deal systems that are PCI only (no ACPI to back up)
like Intel Bay Trail. In order to support such systems, we explicitly bind
setup() to the appropriate DMA filter function and its corresponding parameter.
Then when serial8250_request_dma() doesn't find the channel via ACPI or DT, it
falls back to use the given filter function.
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Acked-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Signed-off-by: Vinod Koul <vinod.koul@intel.com>
The device has a highspeed register which influences the calcualtion
of the divisor. The chip lacks support for some baudrates. When requested,
we set the divisor to the next smaller baudrate and adjust the c_cflag
accordingly.
Signed-off-by: Matthias Brugger <matthias.bgg@gmail.com>
Reviewed-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit: e676253b19 [3/21] serial/8250: Add
support for RS485 IOCTLs, adds a building error on arch m32r.
All error/warnings:
drivers/tty/serial/8250/8250_core.c: In function 'serial8250_ioctl':
>> drivers/tty/serial/8250/8250_core.c:2859:3: error: implicit declaration of function 'copy_from_user' [-Werror=implicit-function-declaration]
if (copy_from_user(&rs485_config, (void __user *)arg,
^
>> drivers/tty/serial/8250/8250_core.c:2871:3: error: implicit declaration of function 'copy_to_user' [-Werror=implicit-function-declaration]
if (copy_to_user((void __user *)arg, &up->rs485,
^
cc1: some warnings being treated as errors
Reported-by: kbuild test robot <fengguang.wu@intel.com>
Signed-off-by: Ricardo Ribalda Delgado <ricardo.ribalda@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Another new ACPI identifier for the 8250 dw bindings to cover newer Intel
SoCs such as Braswell.
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Mika Westerberg <mika.westerberg@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The OMAP version of the 8250 can actually use 1:1 serial8250_startup().
However it needs to be extended by a wake up irq which should to be
requested & enabled at ->startup() time and disabled at ->shutdown() time.
v2…v3: properly copy callbacks
v1…v2: add shutdown callback
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There is no way to access a struct uart_8250_port for a specific
line. This is only required outside of the 8250/uart callbacks like for
devices' suspend & remove callbacks. For those the 8250-core provides a
wrapper like serial8250_unregister_port() which passes the struct
to the proper function based on the line argument.
For run time suspend I need access to this struct not only to make
serial_out() work but also to properly restore up->ier and up->mcr.
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Existing callers of serial8250_modem_status() [1] hold the uart port
lock; document.
[1] In-tree callers of serial8250_modem_status()
drivers/tty/serial/8250/8250_fsl.c
fsl8250_handle_irq()
drivers/tty/serial/8250/8250_core.c
serial8250_handle_irq()
serial8250_console_write()
serial8250_get_mctrl() *
* Call graphs for callers of serial8250_get_mctrl() from the function
which acquires the uart port lock
drivers/tty/serial/serial_core.c
uart_port_startup()
uart_tiocmget()
uart_set_termios()
uart_carrier_raised()
ops->get_mctrl() ---> serial8250_get_mctrl()
Signed-off-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This reverts commit 06aa82e498.
This commit purports to enable auto CTS flow control for the 8250
UART driver. However, the 8250 UART driver already supports auto
CTS flow control via UART_CAP_AFE and UART_CAP_EFR. Indeed, this
patch introduces another DT attribute for which an existing firmware
flag already exists ("auto-flow-control"). Furthermore, the use of
UPF_HARD_FLOW requires the UART driver to define .throttle and
.unthrottle methods, neither of which are defined for the 8250 UART
driver (which will result in a NULL ptr dereference). Finally, this patch
supposes to fix existing bugs in the serial core for auto CTS-enabled
hardware, but does not include the class of hardware for which these
bugs exist.
CC: Murali Karicheri <m-karicheri2@ti.com>
CC: Rob Herring <robh+dt@kernel.org>
Signed-off-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The symbol is defined in drivers/tty/serial/8250/Kconfig as
"SERIAL_8250", not just "8250".
Signed-off-by: Daniele Forsi <dforsi@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This patch lets you set the RS485 cappabilites of the device through
TIOCSRS485 and TIOCGRS485 as defined on Documentation/serial/serial-rs485.txt
In order to probe the device, the PNP id and the device id is used.
Signed-off-by: Ricardo Ribalda Delgado <ricardo.ribalda@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This patch allow the users of the 8250 infrastructure to define a
handler for RS485 configration.
If no handler is defined the 8250 driver will work as usual.
Signed-off-by: Ricardo Ribalda Delgado <ricardo.ribalda@gmail.com>
Acked-by: Alan Cox <alan@linux.intel.com>
--
v2:Change suggested by Alan "One Thousand Gnomes":
- Move rs485 structure further down on the uart_8250_port structure
drivers/tty/serial/8250/8250_core.c | 39 +++++++++++++++++++++++++++++++++++++
include/linux/serial_8250.h | 3 +++
2 files changed, 42 insertions(+)
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add flags field to struct kernel_params, and add the first flag: unsafe
parameter. Modifying a kernel parameter with the unsafe flag set, either
via the kernel command line or sysfs, will issue a warning and taint the
kernel.
Cc: Rusty Russell <rusty@rustcorp.com.au>
Cc: Jean Delvare <khali@linux-fr.org>
Cc: Andrew Morton <akpm@linux-foundation.org>
Cc: Li Zhong <zhong@linux.vnet.ibm.com>
Cc: Jon Mason <jon.mason@intel.com>
Cc: Daniel Vetter <daniel.vetter@ffwll.ch>
Signed-off-by: Jani Nikula <jani.nikula@intel.com>
Signed-off-by: Rusty Russell <rusty@rustcorp.com.au>
The 8250_dw driver fails to probe if the specified clock isn't
registered at probe time. Even if a clock frequency is given,
the required clock might be gated because it wasn't properly
enabled.
This happened to me when the device is registered through DT,
and the clock was part of an MFD, the PRCM found on A31 and A23
SoCs. Unlike core clocks that are registered with OF_CLK_DECLARE,
which happen almost immediately after the kernel starts, the
clocks are registered as sub-devices of the PRCM MFD platform
device. Even though devices are registered in the order they are
found in the DT, the drivers are registered in a different,
arbitrary order. It is possible that the 8250_dw driver is
registered, and thus associated with the device and probed, before
the clock driver is registered and probed.
8250_dw then reports unable to get the clock, and fails. Without
a working console, the kernel panics.
This patch adds support for deferred probe handling for the clock
and reset controller. It also fixes the cleanup path if
serial8250_register_8250_port fails.
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The Allwinner A31 and A23 SoCs have a reset controller
maintaining the UART in reset by default.
This patch adds optional reset support to the driver.
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Acked-by: Maxime Ripard <maxime.ripard@free-electrons.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add tunable RX interrupt trigger I/F of FIFO buffers.
Serial devices are used as not only message communication devices but control
or sending communication devices. For the latter uses, normally small data
will be exchanged, so user applications want to receive data unit as soon as
possible for real-time tendency. If we have a sensor which sends a 1 byte data
each time and must control a device based on the sensor feedback, the RX
interrupt should be triggered for each data.
According to HW specification of serial UART devices, RX interrupt trigger
can be changed, but the trigger is hard-coded. For example, RX interrupt trigger
in 16550A can be set to 1, 4, 8, or 14 bytes for HW, but current driver sets
the trigger to only 8bytes.
This patch makes some devices change RX interrupt trigger from userland.
<How to use>
- Read current setting
# cat /sys/class/tty/ttyS0/rx_trig_bytes
8
- Write user setting
# echo 1 > /sys/class/tty/ttyS0/rx_trig_bytes
# cat /sys/class/tty/ttyS0/rx_trig_bytes
1
<Support uart devices>
- 16550A and Tegra (1, 4, 8, or 14 bytes)
- 16650V2 (8, 16, 24, or 28 bytes)
- 16654 (8, 16, 56, or 60 bytes)
- 16750 (1, 16, 32, or 56 bytes)
<Change log>
Changes in V9:
- Use attr_group instead of dev_spec_attr_group of uart_port structure
Changes in V8:
- Divide this patch from V7's patch based on Greg's comment
Changes in V7:
- Add Documentation
- Change I/F name from rx_int_trig to rx_trig_bytes because the name
rx_int_trig is hard to understand how users specify the value
Changes in V6:
- Move FCR_RX_TRIG_* definition in 8250.h to include/uapi/linux/serial_reg.h,
rename those to UART_FCR_R_TRIG_*, and use UART_FCR_TRIGGER_MASK to
UART_FCR_R_TRIG_BITS()
- Change following function names:
convert_fcr2val() => fcr_get_rxtrig_bytes()
convert_val2rxtrig() => bytes_to_fcr_rxtrig()
- Fix typo in serial8250_do_set_termios()
- Delete the verbose error message pr_info() in bytes_to_fcr_rxtrig()
- Rename *rx_int_trig/rx_trig* to *rxtrig* for several functions or variables
(but UI remains rx_int_trig)
- Change the meaningless variable name 'val' to 'bytes' following functions:
fcr_get_rxtrig_bytes(), bytes_to_fcr_rxtrig(), do_set_rxtrig(),
do_serial8250_set_rxtrig(), and serial8250_set_attr_rxtrig()
- Use up->fcr in order to get rxtrig_bytes instead of rx_trig_raw in
fcr_get_rxtrig_bytes()
- Use conf_type->rxtrig_bytes[0] instead of switch statement for support check
in register_dev_spec_attr_grp()
- Delete the checking whether a user changed FCR or not when minimum buffer
is needed in serial8250_do_set_termios()
Changes in V5.1:
- Fix FCR_RX_TRIG_MAX_STATE definition
Changes in V5:
- Support Tegra, 16650V2, 16654, and 16750
- Store default FCR value to up->fcr when the port is first created
- Add rx_trig_byte[] in uart_config[] for each device and use rx_trig_byte[]
in convert_fcr2val() and convert_val2rxtrig()
Changes in V4:
- Introduce fifo_bug flag in uart_8250_port structure
This is enabled only when parity is enabled and UART_BUG_PARITY is enabled
for up->bugs. If this flag is enabled, user cannot set RX trigger.
- Return -EOPNOTSUPP when it does not support device at convert_fcr2val() and
at convert_val2rxtrig()
- Set the nearest lower RX trigger when users input a meaningless value at
convert_val2rxtrig()
- Check whether p->fcr is existing at serial8250_clear_and_reinit_fifos()
- Set fcr = up->fcr in the begging of serial8250_do_set_termios()
Changes in V3:
- Change I/F from ioctl(2) to sysfs(rx_int_trig)
Changed in V2:
- Use _IOW for TIOCSFIFORTRIG definition
- Pass the interrupt trigger value itself
Signed-off-by: Yoshihiro YUNOMAE <yoshihiro.yunomae.ez@hitachi.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
It helps to cast struct uart_port to struct uart_8250_port at runtime.
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
First try to find the named clock variants then fall back to the already
existing handling of a nameless declared baudclk.
This also adds the missing documentation for this already existing variant.
Signed-off-by: Heiko Stuebner <heiko@sntech.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The flags member has upf_t type and corresponding macros to define them. This
patch converts ASYNC_SKIP_TEST to UPF_SKIP_TEST in 8250_dw.c.
Otherwise we got a sparse warning:
drivers/tty/serial/8250/8250_dw.c:302:46: warning: restricted upf_t degrades to integer
drivers/tty/serial/8250/8250_dw.c:302:62: warning: restricted upf_t degrades to integer
drivers/tty/serial/8250/8250_dw.c:302:26: warning: incorrect type in assignment (different base types)
drivers/tty/serial/8250/8250_dw.c:302:26: expected restricted upf_t [usertype] flags
drivers/tty/serial/8250/8250_dw.c:302:26: got unsigned int
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This replaces the Baytrail specific custom set_termios hook
with a more generic one where the clock framework is used to
set the rate. The method also doesn't need to be limited to
just Baytrail, so it's used with all ACPI platforms.
Signed-off-by: Heikki Krogerus <heikki.krogerus@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In the conversion to generic early console, the passing of options from
the early 8250 console to the regular ttyS console was broken. This
resulted in the baud rate changing when switching consoles during boot.
This feature allows specifying a single console option on the kernel
command line rather than both an early console and regular serial tty
console. It would be nice to generalize this feature. However, it only
works if the correct baud rate can be probed early which is not the
case on many platforms which have non-standard UART clock rates. So for
now, this is left as an 8250 specific feature.
Reported-and-tested-by: Tony Luck <tony.luck@intel.com>
Signed-off-by: Rob Herring <robh@kernel.org>
Cc: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If IGNBRK is set without either BRKINT or PARMRK set, some uart
drivers send a 0x00 byte for BREAK without the TTYBREAK flag to the
line discipline, when it should send either nothing or the TTYBREAK flag
set. This happens because the read_status_mask masks out the BI
condition, which uart_insert_char() then interprets as a normal 0x00 byte.
SUS v3 is clear regarding the meaning of IGNBRK; Section 11.2.2, General
Terminal Interface - Input Modes, states:
"If IGNBRK is set, a break condition detected on input shall be ignored;
that is, not put on the input queue and therefore not read by any
process."
Fix read_status_mask to include the BI bit if IGNBRK is set; the
lsr status retains the BI bit if a BREAK is recv'd, which is
subsequently ignored in uart_insert_char() when masked with the
ignore_status_mask.
Affected drivers:
8250 - all
serial_txx9
mfd
amba-pl010
amba-pl011
atmel_serial
bfin_uart
dz
ip22zilog
max310x
mxs-auart
netx-serial
pnx8xxx_uart
pxa
sb1250-duart
sccnxp
serial_ks8695
sirfsoc_uart
st-asc
vr41xx_siu
zs
sunzilog
fsl_lpuart
sunsab
ucc_uart
bcm63xx_uart
sunsu
efm32-uart
pmac_zilog
mpsc
msm_serial
m32r_sio
Unaffected drivers:
omap-serial
rp2
sa1100
imx
icom
Annotated for fixes:
altera_uart
mcf
Drivers without break detection:
21285
xilinx-uartps
altera_jtaguart
apbuart
arc-uart
clps711x
max3100
uartlite
msm_serial_hs
nwpserial
lantiq
vt8500_serial
Unknown:
samsung
mpc52xx_uart
bfin_sport_uart
cpm_uart/core
Fixes: Bugzilla #71651, '8250_core.c incorrectly handles IGNBRK flag'
Reported-by: Ivan <athlon_@mail.ru>
Signed-off-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Here is the big tty / serial driver pull request for 3.16-rc1.
A variety of different serial driver fixes and updates and additions,
nothing huge, and no real major core tty changes at all.
All have been in linux-next for a while.
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Merge tag 'tty-3.16-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty into next
Pull tty/serial driver updates from Greg KH:
"Here is the big tty / serial driver pull request for 3.16-rc1.
A variety of different serial driver fixes and updates and additions,
nothing huge, and no real major core tty changes at all.
All have been in linux-next for a while"
* tag 'tty-3.16-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty: (84 commits)
Revert "serial: imx: remove the DMA wait queue"
serial: kgdb_nmi: Improve console integration with KDB I/O
serial: kgdb_nmi: Switch from tasklets to real timers
serial: kgdb_nmi: Use container_of() to locate private data
serial: cpm_uart: No LF conversion in put_poll_char()
serial: sirf: Fix compilation failure
console: Remove superfluous readonly check
console: Use explicit pointer type for vc_uni_pagedir* fields
vgacon: Fix & cleanup refcounting
ARM: tty: Move HVC DCC assembly to arch/arm
tty/hvc/hvc_console: Fix wakeup of HVC thread on hvc_kick()
drivers/tty/n_hdlc.c: replace kmalloc/memset by kzalloc
vt: emulate 8- and 24-bit colour codes.
printk/of_serial: fix serial console cessation part way through boot.
serial: 8250_dma: check the result of TX buffer mapping
serial: uart: add hw flow control support configuration
tty/serial: at91: add interrupts for modem control lines
tty/serial: at91: use mctrl_gpio helpers
tty/serial: Add GPIOLIB helpers for controlling modem lines
ARM: at91: gpio: implement get_direction
...
Using dma_mapping_error() to make sure the mapping did not
fail.
Signed-off-by: Heikki Krogerus <heikki.krogerus@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
8250 uart driver currently supports only software assisted hw flow
control. The software assisted hw flow control maintains a hw_stopped
flag in the tty structure to stop and start transmission and use modem
status interrupt for the event to drive the handshake signals. This is
not needed if hw has flow control capabilities. This patch adds a
DT attribute for enabling hw flow control for a uart port. Also skip
stop and start if this flag is present in flag field of the port
structure.
Signed-off-by: Murali Karicheri <m-karicheri2@ti.com>
CC: Rob Herring <robh+dt@kernel.org>
CC: Pawel Moll <pawel.moll@arm.com>
CC: Mark Rutland <mark.rutland@arm.com>
CC: Ian Campbell <ijc+devicetree@hellion.org.uk>
CC: Kumar Gala <galak@codeaurora.org>
CC: Randy Dunlap <rdunlap@infradead.org>
CC: Jiri Slaby <jslaby@suse.cz>
CC: Santosh Shilimkar <santosh.shilimkar@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This Multi-IO card has one serial 16550-like and one parallel port connector.
Here's the lspci output, after this commit is applied:
03:07.0 Serial controller: Device 4348:5053 (rev 10) (prog-if 02 [16550])
Subsystem: Device 4348:5053
Control: I/O+ Mem- BusMaster- SpecCycle- MemWINV- VGASnoop- ParErr- Stepping- SERR- FastB2B- DisINTx-
Status: Cap- 66MHz- UDF- FastB2B- ParErr- DEVSEL=medium >TAbort- <TAbort- <MAbort- >SERR- <PERR- INTx-
Interrupt: pin A routed to IRQ 21
Region 0: I/O ports at cf00 [size=8]
Region 1: I/O ports at ce00 [size=8]
Kernel driver in use: parport_serial
Kernel modules: 8250_pci, parport_serial
This commit adds an entry with the device ID to the blacklist declared in
8250_pci to prevent the driver from taking ownership. Also, and as was done
for the 2S/1P variant, add a quirk to skip autodetection and set the correct
type to 16550A clone.
Proper entries are added to parport_serial, to support the device parallel
and serial ports.
Cc: Gianluca Anzolin <gianluca@sottospazio.it>
Cc: Alan Cox <alan@linux.intel.com>
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Signed-off-by: Ezequiel Garcia <ezequiel.garcia@free-electrons.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>