Step by step, mmc host drivers and the mmc core have been improved in
regards to support erase/discard/trim operations. We have now reached a
point when it no longer seems reasonable to use an opt-in approach to
enable the functionality. Therefore, let's switch to make the operations
always supported.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200508112853.23525-1-ulf.hansson@linaro.org
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Using a fixed 1s polling timeout for all commands is a bit problematic.
For some commands it means waiting longer than needed for the polling to be
aborted, which may not a big issue, but still. For other commands, like for
an erase (CMD38) that uses a R1B response, may require longer timeouts than
1s. In these cases, we may end up treating the command as it failed, while
it just needed some more time to complete successfully.
Fix the problem by respecting the cmd->busy_timeout, which is provided by
the mmc core.
Note that, even if the sdricoh_cs driver may currently not support HW busy
detection on DAT0, some comments in the code refer to that the HW may
support it. Therefore, it seems better to be proactive in this case.
Cc: Sascha Sommer <saschasommer@freenet.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200508095228.14230-1-ulf.hansson@linaro.org
Rather than to poll in a busy-loop, let's convert into using
read_poll_timeout() and insert a small delay between each polling attempts.
In particular, this avoids hogging the CPU.
Additionally, to convert to read_poll_timeout() we also need to switch from
using a specific number of polling attempts, into a specific timeout in us
instead. The previous 100000 attempts, is translated into a total timeout
of total 1s, as that seemed like reasonable value to pick.
Cc: Sascha Sommer <saschasommer@freenet.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200508095218.14177-1-ulf.hansson@linaro.org
Rather than to poll in a busy-loop, let's convert into using
read_poll_timeout() and insert a small delay between each polling attempts.
In particular, this avoids hogging the CPU.
Additionally, to convert to read_poll_timeout() we also need to switch from
using a specific number of polling attempts, into a specific timeout in us
instead. The previous 100000 attempts, is translated into a total timeout
of total 1s, as that seemed like reasonable value to pick.
Cc: Sascha Sommer <saschasommer@freenet.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200508095210.14123-1-ulf.hansson@linaro.org
Some commands uses R1B responses, which means the card may assert the DAT0
line to signal busy for a period of time, after it has received the
command. The mmc core normally specifies the busy period for the command in
the cmd->busy_timeout. Ideally the driver should respect it, but that
requires quite some update of the code, so let's defer that to someone with
the HW at hand.
Instead, let's inform the mmc core about the maximum supported busy timeout
in ->max_busy_timeout during ->probe(). This value corresponds to the fixed
~2s timeout of the polling loop, implemented in cb710_wait_for_event(). In
this way, we let the mmc core validate the needed timeout, which may lead
to that it converts from a R1B into a R1 response and then use CMD13 to
poll for busy completion.
In other words, this change enables support for commands with longer busy
periods than 2s, like erase (CMD38) for example.
Cc: Michał Mirosław <mirq-linux@rere.qmqm.pl>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200414161413.3036-7-ulf.hansson@linaro.org
The current codebase makes use of the zero-length array language
extension to the C90 standard, but the preferred mechanism to declare
variable-length types such as these ones is a flexible array member[1][2],
introduced in C99:
struct foo {
int stuff;
struct boo array[];
};
By making use of the mechanism above, we will get a compiler warning
in case the flexible array does not occur last in the structure, which
will help us prevent some kind of undefined behavior bugs from being
inadvertently introduced[3] to the codebase from now on.
Also, notice that, dynamic memory allocations won't be affected by
this change:
"Flexible array members have incomplete type, and so the sizeof operator
may not be applied. As a quirk of the original implementation of
zero-length arrays, sizeof evaluates to zero."[1]
sizeof(flexible-array-member) triggers a warning because flexible array
members have incomplete type[1]. There are some instances of code in
which the sizeof operator is being incorrectly/erroneously applied to
zero-length arrays and the result is zero. Such instances may be hiding
some bugs. So, this work (flexible-array member conversions) will also
help to get completely rid of those sorts of issues.
This issue was found with the help of Coccinelle.
[1] https://gcc.gnu.org/onlinedocs/gcc/Zero-Length.html
[2] https://github.com/KSPP/linux/issues/21
[3] commit 7649773293 ("cxgb3/l2t: Fix undefined behaviour")
Signed-off-by: Gustavo A. R. Silva <gustavoars@kernel.org>
Link: https://lore.kernel.org/r/20200507192218.GA16315@embeddedor
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The 'pengutronix' address is defunct for years. Use the proper contact
address.
Signed-off-by: Wolfram Sang <wsa@kernel.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/20200502142840.19418-1-wsa@kernel.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Following eMMC JEDEC JESD84-B51 standard, an enhanced form of
rpmb is supported. What this enhanced mode supports is in addition
to be able to write one rpmb or two rpmb frames at a time,
32 frames can be written at a time.
Expose this information present in ext csd field so that the
user space application that wants to make use of this can do so.
Signed-off-by: Krishna Konda <kkonda@codeaurora.org>
Signed-off-by: Veerabhadrarao Badiganti <vbadigan@codeaurora.org>
Link: https://lore.kernel.org/r/1588341189-4371-1-git-send-email-vbadigan@codeaurora.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
According to the comment in mmc_sdio_reinit_card(), some SDIO cards may
require a "[CMD5,5,3,7] init sequence", which isn't always obeyed in
mmc_sdio_init_card(). Especially, when we end up retrying the UHS-I
specific initialization, there is a missing CMD5.
Let's update the code to make the behaviour consistent and let's also take
the opportunity to clean up the code a bit, to avoid open coding.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200430091640.455-5-ulf.hansson@linaro.org
While initializing an SDIO card in mmc_sdio_init_card(), we may need to
retry the UHS-I specific initialization, in case the first attempt fails.
This leads to resending a CMD8, but also to restart from scratch with the
so called OCR mask negotiations. This is unnecessary as we already have a
negotiated OCR mask, so let's use that instead. In this way, the behaviour
also becomes more consistent with other similar paths.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200430091640.455-4-ulf.hansson@linaro.org
Over the years, the code in mmc_sdio_init_card() has grown to become quite
messy. Unfortunate this has also lead to that several paths are leaking
memory in form of an allocated struct mmc_card, which includes additional
data, such as initialized struct device for example.
Unfortunate, it's a too complex task find each offending commit. Therefore,
this change fixes all memory leaks at once.
Cc: <stable@vger.kernel.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200430091640.455-3-ulf.hansson@linaro.org
During some scenarios mmc_sdio_init_card() runs a retry path for the UHS-I
specific initialization, which leads to removal of the previously allocated
card. A new card is then re-allocated while retrying.
However, in one of the corresponding error paths we may end up to remove an
already removed card, which likely leads to a NULL pointer exception. So,
let's fix this.
Fixes: 5fc3d80ef4 ("mmc: sdio: don't use rocr to check if the card could support UHS mode")
Cc: <stable@vger.kernel.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200430091640.455-2-ulf.hansson@linaro.org
Even though specifying OPP's in device tree is optional, ignoring all errors
reported by dev_pm_opp_of_add_table() means we can't distinguish between a
missing OPP table and a wrong/buggy OPP table. While missing OPP table
(dev_pm_opp_of_add_table() returns a -ENODEV in such case) can be ignored,
a wrong/buggy OPP table in device tree should make the driver error out.
while we fix that, lets also fix the variable names for opp/opp_table to
avoid confusion and name them opp_table/has_opp_table instead.
Suggested-by: Matthias Kaehlcke <matthias@chromium.org>
Signed-off-by: Rajendra Nayak <rnayak@codeaurora.org>
Link: https://lore.kernel.org/r/1588080785-6812-10-git-send-email-rnayak@codeaurora.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
With R-Car Gen3, CRC error occue at the following TAPs.
H3, M3W 1.3, M3N... TAP=2,3,6,7
M3W 3.0 ... TAP=1,3,5,7
(Note: for 4tap SoCs, the numbers get divided by 2)
Do not use these TAPs in HS400, and also don't use auto correction but
manual correction.
We check for bad taps in two places:
1) After tuning HS400: Then, we select a neighbouring TAP. One of them
must be good, because there are never three bad taps in a row.
Retuning won't help because we just finished tuning.
2) After a manual correction request: Here, we can't switch to the
requested TAP. But we can retune (if the HS200 tuning was good)
because the environment might have changed since the last tuning.
If not, we stay on the same TAP.
Signed-off-by: Takeshi Saito <takeshi.saito.xv@renesas.com>
[wsa: refactored to match upstream driver, reworded commit msg]
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20200423130432.9990-3-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
For ES1.2, add a comment explaining the situation. For ES1.3 (and
later, although unlikely), add a new entry defining it as 4tap.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20200423130432.9990-2-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Using a fixed 3s polling timeout for all commands with R1B responses is a
bit problematic.
For some commands it means waiting longer than needed for the polling to be
aborted, which may not a big issue, but still. For other commands, like for
an erase (CMD38), may require longer timeouts than 3s. In these cases, we
may end up treating the command as it failed, while it just needed some
more time to complete successfully.
Fix the problem by respecting the cmd->busy_timeout, which is provided by
the mmc core.
Cc: Jonathan Neuschäfer <j.neuschaefer@gmx.net>
Cc: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200414161413.3036-19-ulf.hansson@linaro.org
Clarify the use of r1b_timeout, by renaming it to MMC_SPI_R1B_TIMEOUT_MS
and by dropping the corresponding confusing comment about it.
Additionally, let's also add a new define, MMC_SPI_INIT_TIMEOUT_MS and use
it during the initialization. Even if these two defines are given the same
value, the split makes it easier to understand them.
Cc: Jonathan Neuschäfer <j.neuschaefer@gmx.net>
Cc: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200414161413.3036-18-ulf.hansson@linaro.org
Using a fixed 1s timeout for all commands (and data transfers) is a bit
problematic.
For some commands it means waiting longer than needed for the timer to
expire, which may not a big issue, but still. For other commands, like for
an erase (CMD38) that uses a R1B response, may require longer timeouts than
1s. In these cases, we may end up treating the command as it failed, while
it just needed some more time to complete successfully.
Fix the problem by respecting the cmd->busy_timeout, which is provided by
the mmc core.
Cc: Bruce Chang <brucechang@via.com.tw>
Cc: Harald Welte <HaraldWelte@viatech.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200414161413.3036-17-ulf.hansson@linaro.org
Some commands uses R1B responses, which means the card may assert the DAT0
line to signal busy for a period of time, after it has received the
command. The mmc core normally specifies the busy period for the command in
the cmd->busy_timeout. Ideally the driver should respect it, but that
requires quite some update of the code, so let's defer that to someone with
the HW at hand.
Instead, let's inform the mmc core about the maximum supported busy timeout
in ->max_busy_timeout during ->probe(). This value corresponds to the fixed
1s timeout used by tifm_sd. In this way, we let the mmc core validate the
needed timeout, which may lead to that it converts from a R1B into a R1
response and then use CMD13 to poll for busy completion.
In other words, this change enables support for commands with longer busy
periods than 1s, like erase (CMD38) for example.
Cc: Alex Dubov <oakad@yahoo.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200414161413.3036-16-ulf.hansson@linaro.org
The in-parameter timeout is always set to TRANSFER_TIMEOUT by the callers
of sdricoh_query_status(), hence let's drop it.
Cc: Sascha Sommer <saschasommer@freenet.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200414161413.3036-12-ulf.hansson@linaro.org
For commands that doesn't involve to prepare a data transfer, owl-mmc is
using a fixed 30s response timeout. This is a bit problematic.
For some commands it means waiting longer than needed for the completion to
expire, which may not a big issue, but still. For other commands, like for
an erase (CMD38) that uses a R1B response, may require longer timeouts than
30s. In these cases, we may end up treating the command as it failed, while
it just needed some more time to complete successfully.
Fix the problem by respecting the cmd->busy_timeout, which is provided by
the mmc core.
Cc: Manivannan Sadhasivam <manivannan.sadhasivam@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200414161413.3036-8-ulf.hansson@linaro.org
Some commands uses R1B responses, which means the card may assert the DAT0
line to signal busy for a period of time, after it has received the
command. The mmc core normally specifies the busy period for the command in
the cmd->busy_timeout. Ideally the driver should respect it, but that
requires quite some update of the code, so let's defer that to someone with
the HW at hand.
Instead, let's inform the mmc core about the maximum supported busy timeout
in ->max_busy_timeout during ->probe(). This value corresponds to the fixed
5s timeout used by jz4740. In this way, we let the mmc core validate the
needed timeout, which may lead to that it converts from a R1B into a R1
response and then use CMD13 to poll for busy completion.
In other words, this change enables support for commands with longer busy
periods than 5s, like erase (CMD38) for example.
Cc: Paul Cercueil <paul@crapouillou.net>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Link: https://lore.kernel.org/r/20200414161413.3036-5-ulf.hansson@linaro.org
Fix the following sparse warning:
drivers/mmc/host/sdhci-pci-o2micro.c:497:6: warning: symbol
'sdhci_pci_o2_set_clock' was not declared. Should it be static?
drivers/mmc/host/sdhci-pci-o2micro.c:512:5: warning: symbol
'sdhci_pci_o2_probe_slot' was not declared. Should it be static?
drivers/mmc/host/sdhci-pci-o2micro.c:581:5: warning: symbol
'sdhci_pci_o2_probe' was not declared. Should it be static?
drivers/mmc/host/sdhci-pci-o2micro.c:786:5: warning: symbol
'sdhci_pci_o2_resume' was not declared. Should it be static?
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Zou Wei <zou_wei@huawei.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/1587624199-96926-1-git-send-email-zou_wei@huawei.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Fixes coccicheck warning:
drivers/mmc/core/debugfs.c:222:0-23: WARNING: mmc_clock_fops should be
defined with DEFINE_DEBUGFS_ATTRIBUTE
Use DEFINE_DEBUGFS_ATTRIBUTE rather than DEFINE_SIMPLE_ATTRIBUTE
for debugfs files
Fixes: 703aae3d09 ("mmc: add a file to debugfs for changing host clock at runtime")
Fixes: a04c50aaa9 ("mmc: core: no need to check return value of debugfs_create functions")
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Zou Wei <zou_wei@huawei.com>
Link: https://lore.kernel.org/r/1587633319-19835-1-git-send-email-zou_wei@huawei.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
If sdhci-of-at91.c is compiled without CONFIG_HAVE_CLK, the line
caps1 |= FIELD_PREP(SDHCI_CLOCK_MUL_MASK, clk_mul);
... emits "FIELD_PREP: value too large for the field" warning.
The compiler seems to decide clk_mul is constant (unsigned int)-1,
because clk_get_rate() returns 0 when CONFIG_HAVE_CLK is disabled.
Add HAVE_CLK to the depenency since this driver does not work without
the clock APIs anyway.
Reported-by: Randy Dunlap <rdunlap@infradead.org>
Suggested-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Link: https://lore.kernel.org/r/20200422153401.7913-1-yamada.masahiro@socionext.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Randy Dunlap <rdunlap@infradead.org> # build-tested
After TAP refactorization, we can use 'unsigned int' for two more
variables because all the calculations work on this type now.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Niklas Söderlund <niklas.soderlund+renesas@ragnatech.se>
Link: https://lore.kernel.org/r/20200420170230.9091-1-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch fix a power-on issue, and avoid to retry the power sequence.
In power off sequence: sdmmc must set pwr_reg in "power-cycle" state
(value 0x2), to prevent the card from being supplied through the signal
lines (all the lines are driven low).
In power on sequence: when the power is stable, sdmmc must set pwr_reg
in "power-off" state (value 0x0) to drive all signal to high before to
set "power-on".
To avoid writing the same value to the power register several times, this
register is cached by the pwr_reg variable. At probe pwr_reg is initialized
to 0 by kzalloc of mmc_alloc_host.
Like pwr_reg value is 0 at probing, the power on sequence fail because
the "power-off" state is not writes (value 0x0) and the lines
remain drive to low.
This patch initializes "pwr_reg" variable with power register value.
This it done in sdmmc variant init to not disturb default mmci behavior.
Signed-off-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200420161831.5043-1-ludovic.barre@st.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
On some qualcomm SoCs we need to vote on a performance state of a power
domain depending on the clock rates. Hence move to using OPP api to set
the clock rate and performance state specified in the OPP table.
On platforms without an OPP table, dev_pm_opp_set_rate() is eqvivalent to
clk_set_rate()
Signed-off-by: Rajendra Nayak <rnayak@codeaurora.org>
Link: https://lore.kernel.org/r/1587132279-27659-10-git-send-email-rnayak@codeaurora.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Using a fixed 1s timeout for all commands is a bit problematic.
For some commands it means waiting longer than needed for the timeout to
expire, which may not a big issue, but still. For other commands, like for
an erase (CMD38) that uses a R1B response, may require longer timeouts than
1s. In these cases, we may end up treating the command as it failed, while
it just needed some more time to complete successfully.
Fix the problem by respecting the cmd->busy_timeout, which is provided by
the mmc core.
Cc: Rui Miguel Silva <rmfrfs@gmail.com>
Cc: Johan Hovold <johan@kernel.org>
Cc: Alex Elder <elder@kernel.org>
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Cc: greybus-dev@lists.linaro.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Rui Miguel Silva <rmfrfs@gmail.com>
Acked-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Link: https://lore.kernel.org/r/20200414161413.3036-20-ulf.hansson@linaro.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some commands uses R1B responses, which means the card may assert the DAT0
line to signal busy for a period of time, after it has received the
command. The mmc core normally specifies the busy period for the command in
the cmd->busy_timeout. Ideally the driver should respect it, but that
requires quite some update of the code, so let's defer that to someone with
the HW at hand.
Instead, let's inform the mmc core about the maximum supported busy timeout
in ->max_busy_timeout during ->probe(). This value corresponds to the fixed
4s timeout used by usdhi6rol0. In this way, we let the mmc core validate
the needed timeout, which may lead to that it converts from a R1B into a R1
response and then use CMD13 to poll for busy completion.
In other words, this change enables support for commands with longer busy
periods than 4s, like erase (CMD38) for example.
Cc: Jesper Nilsson <jesper.nilsson@axis.com>
Cc: Lars Persson <lars.persson@axis.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Jesper Nilsson <jesper.nilsson@axis.com>
Link: https://lore.kernel.org/r/20200414161413.3036-6-ulf.hansson@linaro.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Using a fixed 2s timeout for all commands is a bit problematic.
For some commands it means waiting longer than needed for the timer to
expire, which may not a big issue, but still. For other commands, like for
an erase (CMD38) that uses a R1B response, may require longer timeouts than
2s. In these cases, we may end up treating the command as it failed, while
it just needed some more time to complete successfully.
Fix the problem by respecting the cmd->busy_timeout, which is provided by
the mmc core.
Cc: Ludovic Desroches <ludovic.desroches@microchip.com>
Cc: Nicolas Ferre <nicolas.ferre@microchip.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Ludovic Desroches <ludovic.desroches@microchip.com>
Link: https://lore.kernel.org/r/20200414161413.3036-4-ulf.hansson@linaro.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Setting the timer on a per request basis, is rather limiting as the timer
really depends on what commands that is to be sent as part of the request.
Therefore improve the behaviour by programming the timer per command basis
instead.
Cc: Ludovic Desroches <ludovic.desroches@microchip.com>
Cc: Nicolas Ferre <nicolas.ferre@microchip.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Ludovic Desroches <ludovic.desroches@microchip.com>
Link: https://lore.kernel.org/r/20200414161413.3036-3-ulf.hansson@linaro.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When atmci_request_end() is about to finish a request for one slot, there
is a possibility that there is new request queued for another slot. If this
turns out to be the case, the new request is started and the timer is
re-programmed for it.
Although, a few lines below in atmci_request_end(), this timer becomes
deleted, likely corresponding to the other recently completed request. This
looks wrong, so let's fix it.
Cc: Ludovic Desroches <ludovic.desroches@microchip.com>
Cc: Nicolas Ferre <nicolas.ferre@microchip.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Ludovic Desroches <ludovic.desroches@microchip.com>
Link: https://lore.kernel.org/r/20200414161413.3036-2-ulf.hansson@linaro.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
ADMA_ERR_SIZE_EN bit of VENDOR_SPECIFIC_FUNC register controls
ADMA length mismatch error interrupt. Enable it by default.
And update all bit shift defines with BIT macro.
Signed-off-by: Veerabhadrarao Badiganti <vbadigan@codeaurora.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/1587363626-20413-4-git-send-email-vbadigan@codeaurora.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
sdhci-msm can support auto cmd12.
So enable SDHCI_QUIRK_MULTIBLOCK_READ_ACMD12 quirk.
Signed-off-by: Veerabhadrarao Badiganti <vbadigan@codeaurora.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/1587363626-20413-3-git-send-email-vbadigan@codeaurora.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When use one SDIO wifi which enable the runtime PM feature on i.MX6SX,
we meet system hang. This hang happened during the usdhc runtime resume,
in sdhci_init(), when call the sdhci_set_default_irqs. One interrupt
(SDHCI_INT_CARD_INT) triggered just after the host->ier update and before
the write of register SDHCI_SIGNAL_ENABLE. So in sdhci_irq, it will skip
the call of sdio_signal_irq() because current host->ier do not set the
SDHCI_INT_CARD_INT. So this SDIO wifi interrupt always keep triggered,
let the system stuck in irq handle, can't response any other thread.
This patch add spin lock for the sdhci_set_default_irqs to fix this issue.
Signed-off-by: Haibo Chen <haibo.chen@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/1586941255-9237-1-git-send-email-haibo.chen@nxp.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Implement the request_atomic() API for nonremovable cards, that means
we can submit next request in the irq hard handler context to reduce
latency.
Moreover factor out the AUTO CMD23 checking into a separate function
to reduce duplicate code.
Signed-off-by: Baolin Wang <baolin.wang7@gmail.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/60142fe6c6c1dbba2696e775564ae2166786f0bc.1586744073.git.baolin.wang7@gmail.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Implement the request_atomic() ops for the sdhci driver to process
one request in the atomic context if the card is nonremovable.
Moreover, we should return BUSY flag if controller has not released
the inhibit bits to allow HSQ trying to send request again in non-atomic
context.
Suggested-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Baolin Wang <baolin.wang7@gmail.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/9ed34afa9fb42e0c234065cac5401d7826942b55.1586744073.git.baolin.wang7@gmail.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The SD host controller can process one request in the atomic context if
the card is nonremovable, which means we can submit next request in the
irq hard handler when using the MMC host software queue to reduce the
latency. Thus this patch adds a new API request_atomic() for the host
controller, as well as adding support for host software queue to submit
a request by the new request_atomic() API.
Moreover there is an unusual case that the card is busy when trying to
send a command, and we can not polling the card status in interrupt
context by using request_atomic() to dispatch requests. Thus we should
queue a work to try again in the non-atomic context in case the host
releases the busy signal later.
Suggested-by: Adrian Hunter <adrian.hunter@intel.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/a344e27e506cb2329073cbd5cf65e15cc3cbeba9.1586744073.git.baolin.wang7@gmail.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Spending time under spinlock increases IRQ latencies and also
response times because preemption is disabled.
sdhci_send_command() waits up to 10 ms under spinlock for inhibit bits
to clear. In general inhibit bits will not be set, but there may be
corner cases, especially in the face of errors, where waiting helps.
There might also be dysfunctional hardware that needs the waiting. So
retain the legacy behaviour but do not wait for inhibit bits while under
spinlock. Instead adjust the logic to enable waiting while not under
spinlock. That is mostly straight forward, but in the interrupt handler
it requires deferring an "inhibited" command to the IRQ thread where
sleeping is allowed.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/20200412090349.1607-6-adrian.hunter@intel.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In preparation for further changes, tidy sdhci_request() a bit.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/20200412090349.1607-5-adrian.hunter@intel.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
sdhci_finish_data() is defined before it is referenced, so forward
declaration is not necessary.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/20200412090349.1607-4-adrian.hunter@intel.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
sdhci_send_command() has not been used outside of sdhci.c for many
years. Stop exporting it.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/20200412090349.1607-3-adrian.hunter@intel.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Add 2 helper functions to make the use of the auto-CMD23 flag more
readable.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/20200412090349.1607-2-adrian.hunter@intel.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Use the well defined HIGH_SPEED_BUS_SPEED macro in mmc_sd_switch_hs()
to make code more readable.
Signed-off-by: Jisheng Zhang <Jisheng.Zhang@synaptics.com>
Link: https://lore.kernel.org/r/20200410145643.630b0731@xhacker.debian
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>