In case that CONFIG_SLUB_DEBUG is on and pty is used, races between
release_one_tty and flush_to_ldisc work threads may happen and lead
to use-after-free condition on tty->link->port. Because SLUB_DEBUG
is turned on, freed tty->link->port is filled with POISON_FREE value.
So far without SLUB_DEBUG, port was filled with zero and flush_to_ldisc
could return without a problem by checking if tty is NULL.
CPU 0 CPU 1
----- -----
release_tty pty_write
cancel_work_sync(tty) to = tty->link
tty_kref_put(tty->link) tty_schedule_flip(to->port)
<< workqueue >> ...
release_one_tty ...
pty_cleanup ...
kfree(tty->link->port) << workqueue >>
flush_to_ldisc
tty = READ_ONCE(port->itty)
tty is 0x6b6b6b6b6b6b6b6b
!!PANIC!! access tty->ldisc
Unable to handle kernel paging request at virtual address 6b6b6b6b6b6b6b93
pgd = ffffffc0eb1c3000
[6b6b6b6b6b6b6b93] *pgd=0000000000000000, *pud=0000000000000000
------------[ cut here ]------------
Kernel BUG at ffffff800851154c [verbose debug info unavailable]
Internal error: Oops - BUG: 96000004 [#1] PREEMPT SMP
CPU: 3 PID: 265 Comm: kworker/u8:9 Tainted: G W 3.18.31-g0a58eeb #1
Hardware name: Qualcomm Technologies, Inc. MSM 8996pro v1.1 + PMI8996 Carbide (DT)
Workqueue: events_unbound flush_to_ldisc
task: ffffffc0ed610ec0 ti: ffffffc0ed624000 task.ti: ffffffc0ed624000
PC is at ldsem_down_read_trylock+0x0/0x4c
LR is at tty_ldisc_ref+0x24/0x4c
pc : [<ffffff800851154c>] lr : [<ffffff800850f6c0>] pstate: 80400145
sp : ffffffc0ed627cd0
x29: ffffffc0ed627cd0 x28: 0000000000000000
x27: ffffff8009e05000 x26: ffffffc0d382cfa0
x25: 0000000000000000 x24: ffffff800a012f08
x23: 0000000000000000 x22: ffffffc0703fbc88
x21: 6b6b6b6b6b6b6b6b x20: 6b6b6b6b6b6b6b93
x19: 0000000000000000 x18: 0000000000000001
x17: 00e80000f80d6f53 x16: 0000000000000001
x15: 0000007f7d826fff x14: 00000000000000a0
x13: 0000000000000000 x12: 0000000000000109
x11: 0000000000000000 x10: 0000000000000000
x9 : ffffffc0ed624000 x8 : ffffffc0ed611580
x7 : 0000000000000000 x6 : ffffff800a42e000
x5 : 00000000000003fc x4 : 0000000003bd1201
x3 : 0000000000000001 x2 : 0000000000000001
x1 : ffffff800851004c x0 : 6b6b6b6b6b6b6b93
Signed-off-by: Sahara <keun-o.park@darkmatter.ae>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Prior to this patch, the code would happily trigger TX on some ports
before having a chance of reading the RX buffer from the rest of them.
When no flow control was used, this led to RX buffer overruns and
therefore lost data under certain circumstances.
I was able to reproduce this with MAX14830 (that's a quad channel one)
and a simple daisy-chain of RX and TX ports on the eval board:
- TX0 -> RX1
- TX1 -> RX2
- TX2 -> RX3
- TX3 -> RX0
I was testing this by transferring 2MB of data at 115200 baud via each
port. I used a Solidrun Clearfog Base (Armada 388) which was talking to
the UART over an SPI bus clocked at 26MHz (the chip's maximum). Without
this patch, I would always get a "Possible RX FIFO overrun" in dmesg,
and fewer-than-expected amount of bytes received over ttyMAX0. Results
on ttyMAX{1,2,3} tended to be correct all the time, even without the
previous patches in this series and with PIO SPI transfers ("indirect
mode" as the Marvell datasheet calls it), so I assume that heavy
congestion is needed in order to reproduce this.
A drawback of this patch is that the throughput gets reduced "a bit".
Previously, a 115200 baud resulted in about 11.2kBps throughput as
reported by a simple `pv`. With this patch, the throughput of four
parallel streams is roughly 7kBps each, and 9kBps for three streams.
There is no slowdown for one or two parallel streams.
Situation is worse if bytes are being read one-by-one (such as if the
userspace wants to perform parity/framing/break checking) and therefore
without the batched reads.
With just this patch and no other modifications on top of 4.14, I was
only getting roughly 3.6kBps with four parallel streams. The
single-stream performance was the same, and I was seeing about 7.2kBps
with two parallel streams. `perf top` said that a substantial amount of
time was spent in `finish_task_switch`, `_raw_spin_unlock_irqrestore`
and `__timer_delay`.
Signed-off-by: Jan Kundrát <jan.kundrat@cesnet.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The hardware has a 128 byte RX FIFO buffer for each independent UART.
Previously, the code was always reading that byte-by-byte via
independent SPI transactions and the associated overhead. In practice,
this led to up to eight bytes over SPI for just one byte in the UART's
RX FIFO:
- reading the global IRQ register (two bytes, one for command, the other
for data)
- reading one UART's ISR (again two bytes)
- reading the byte count (two bytes yet again)
- finally, reading one byte of the FIFO via another two-byte transaction
We cannot always use a batched read. If the TTY is set to intercept
break conditions or report framing or parity errors, then it is required
to check the Line Status Register (LSR) for each byte which is read from
the RX FIFO. The documentation does not show a way of doing that in a
single SPI transaction; registers 0x00 and 0x04 are separate.
In my testing, this is no silver bullet. I was feeding 2MB of random
data over four daisy-chaned UARTs of MAX14830, and this is the
distribution that I was getting:
- R <= 1: 7437322
- R <= 2: 162093
- R <= 4: 4093
- R <= 8: 4196
- R <= 16: 645
- R <= 32: 165
- R <= 64: 58
- R <= 128: 0
For a reference, batching the write operations works much better:
- W <= 1: 2664
- W <= 2: 1305
- W <= 4: 627
- W <= 8: 371
- W <= 16: 121
- W <= 32: 68
- W <= 64: 33
- W <= 128: 63139
That's probably because this HW/SW combination (Clearfog Base, Armada
388) is probably "good enough" to react to the chip's IRQ "fast enough"
most of the time. Still, I was getting RX overruns every now and then.
In future, I plan to improve this by letting the RX FIFO be filled a
little more (the chip has support for that and also for a "stale
timeout" to prevent additional starvation).
Signed-off-by: Jan Kundrát <jan.kundrat@cesnet.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The transmit register supports batched writes. The key is simply to keep
sending additional bytes up to the FIFO size in the same SPI
transaction with the CS pin still being held low.
This duplicates the regmap infrastructure to a certain extent. There are
some provisions for multiple writes in there, but there does not appear
to be any support for those writes which are destined to the *same*
register (and also no standard for SPI bus transfers of these, anyway).
This patch does not solve every case (if the UART xmit circular buffer
wraps around, we're still doing two SPI transactions), but at least
it's not one-byte-per-transaction anymore.
This change does not touch the receive path at this time. Doing that in
the generic case appears to be impossible in the general case, because
the chips' status register contains data about the *current* byte in the
HW's Rx FIFO. We cannot read these two registers in one go,
unfortunately.
Signed-off-by: Jan Kundrát <jan.kundrat@cesnet.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
According to my chip's datasheet [1], the IRQ output is an open
collector pin which is suitable for sharing with other chips. The chip
also has a register which indicates which UART performed a change and
the driver checks that register already, so we have everything what is
needed to effectively share the IRQ GPIO.
[1] https://datasheets.maximintegrated.com/en/ds/MAX14830.pdf
Signed-off-by: Jan Kundrát <jan.kundrat@cesnet.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
As suggested by Russell King, a driver should not really care about bits
such as the interrupt polarity or whether it is edge- or level-
triggered. The reasons for that include:
- an upstream IRQ controller which cannot support edge- or
level-triggered interrupts,
- board design with a built-in inverter
The interrupt type is being already specified by the Device Tree,
anyway. Other drivers (gpio/gpio-tc3589x.c for example) already work in
this way, delegating the proper IRQ line setup to the DT and not
specifying anything by hand.
Also, there's no reason to have the IRQ flags split between two places.
The SPI probing is the only entry point anyway.
Signed-off-by: Jan Kundrát <jan.kundrat@cesnet.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Serdev does not use the file abstraction and specifically there will
never be anyone polling a file descriptor for POLLOUT events.
Just use plain wake_up_interruptible() in the write_wakeup callback and
document why it's there.
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When compile-testing an allmodconfig kernel for a platform without
sh-sci serial ports, the SERIAL_SH_SCI_NR_UARTS symbol of type "int"
doesn't get assigned a numerical default value, but an empty string,
leading to a build failure:
.config:3814:warning: symbol value '' invalid for SERIAL_SH_SCI_NR_UARTS
...
make[3]: *** [silentoldconfig] Error 1
Fix this by explicitly providing a default value of 2, like before.
Reported-by: kbuild test robot <fengguang.wu@intel.com>
Fixes: f6731485a5 ("tty: serial: sh-sci: Hide number of ports config question")
Signed-off-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The `max310x_spi_probe` function attempted to setup the GPIO bits before
the corresponding structs for each serial port were initialized. If the
DTS file specified a GPIO hog, this led to a crash because the GPIO
stack ended up calling `max310x_gpio_direction_output` which referenced
uninitialized memory:
[<c04598c0>] (max310x_gpio_direction_output) from [<c03f5a2c>] (_gpiod_direction_output_raw+0x94/0x2d4)
[<c03f5a2c>] (_gpiod_direction_output_raw) from [<c03f991c>] (gpiod_hog+0x6c/0x154)
[<c03f991c>] (gpiod_hog) from [<c03fa2d8>] (of_gpiochip_add+0x28c/0x444)
[<c03fa2d8>] (of_gpiochip_add) from [<c03f6b2c>] (gpiochip_add_data+0x4f8/0x760)
[<c03f6b2c>] (gpiochip_add_data) from [<c03f6dd4>] (devm_gpiochip_add_data+0x40/0x7c)
[<c03f6dd4>] (devm_gpiochip_add_data) from [<c0459fec>] (max310x_spi_probe+0x530/0x894)
[<c0459fec>] (max310x_spi_probe) from [<c0503294>] (spi_drv_probe+0x7c/0xac)
[<c0503294>] (spi_drv_probe) from [<c046628c>] (driver_probe_device+0x234/0x2e8)
[<c046628c>] (driver_probe_device) from [<c0464890>] (bus_for_each_drv+0x60/0x94)
[<c0464890>] (bus_for_each_drv) from [<c0465f78>] (__device_attach+0xb0/0x114)
[<c0465f78>] (__device_attach) from [<c0465548>] (bus_probe_device+0x84/0x8c)
[<c0465548>] (bus_probe_device) from [<c0463a00>] (device_add+0x3f4/0x580)
[<c0463a00>] (device_add) from [<c0504164>] (spi_add_device+0x9c/0x134)
[<c0504164>] (spi_add_device) from [<c0504c18>] (spi_register_controller+0x484/0x910)
[<c0504c18>] (spi_register_controller) from [<c0506ee0>] (orion_spi_probe+0x2f4/0x3b4)
[<c0506ee0>] (orion_spi_probe) from [<c0467dac>] (platform_drv_probe+0x50/0xb0)
[<c0467dac>] (platform_drv_probe) from [<c046628c>] (driver_probe_device+0x234/0x2e8)
[<c046628c>] (driver_probe_device) from [<c04663f8>] (__driver_attach+0xb8/0xbc)
[<c04663f8>] (__driver_attach) from [<c04647e8>] (bus_for_each_dev+0x68/0x9c)
[<c04647e8>] (bus_for_each_dev) from [<c046574c>] (bus_add_driver+0x104/0x210)
[<c046574c>] (bus_add_driver) from [<c0466f14>] (driver_register+0x78/0xf4)
[<c0466f14>] (driver_register) from [<c0101bdc>] (do_one_initcall+0x44/0x168)
[<c0101bdc>] (do_one_initcall) from [<c0a00dc0>] (kernel_init_freeable+0x140/0x1cc)
[<c0a00dc0>] (kernel_init_freeable) from [<c078c590>] (kernel_init+0x8/0x108)
[<c078c590>] (kernel_init) from [<c0107a50>] (ret_from_fork+0x14/0x24)
This can be easily fixed by moving the corresponding code below. And
because the UARTs are already there by the time we reach this point, the
`goto` needs changing so that more stuff is freed. (I have not tested
this error path.)
Signed-off-by: Jan Kundrát <jan.kundrat@cesnet.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If uart_add_one_port() fails in mxs_auart_probe, the clks has
to be disabled.Two clks are previously enabled in mxs_get_clks().
Found by Linux Driver Verification project (linuxtesting.org).
Signed-off-by: Branislav Radocaj <branislav@radocaj.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit 3840ed9548 ("tty: goldfish: Implement support for kernel
'earlycon' parameter") breaks an allmodconfig config on x86:
| LD vmlinux.o
| MODPOST vmlinux.o
|drivers/tty/serial/earlycon.o: In function `parse_options':
|drivers/tty/serial/earlycon.c:97: undefined reference to `uart_parse_earlycon'
|Makefile:1005: recipe for target 'vmlinux' failed
earlycon.c::parse_options() invokes uart_parse_earlycon() from serial_core.c
which is compiled=m because GOLDFISH_TTY itself (and most others) are =m.
To avoid that, I'm adding the _CONSOLE config option which is selected if the
GOLDFISH module itself is =y since it doesn't need the early bits for the =m
case (other drivers do the same dance).
The alternative would be to move uart_parse_earlycon() from
serial_core.c to earlycon.c (we don't have that many users of that
function).
Fixes: 3840ed9548 ("tty: goldfish: Implement support for kernel
'earlycon' parameter")
Signed-off-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Reviewed-by: Miodrag Dinic <miodrag.dinic@mips.com>
Acked-by: Miodrag Dinic <miodrag.dinic@mips.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Fixed a spelling error in a comment.
Signed-off-by: Rolf Evers-Fischer <rolf.evers.fischer@aptiv.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If there is no clock rate for uartclk defined, disable the previously
enabled clock again.
Found by Linux Driver Verification project (linuxtesting.org).
Fixes: 23f5b3fdd0 serial: 8250_dw: only get the clock rate in one place
Signed-off-by: Stefan Potyra <Stefan.Potyra@elektrobit.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The driver may sleep under a spinlock.
The function call paths are:
isicom_activate (acquire the spinlock)
isicom_setup_board
drop_dtr_rts
WaitTillCardIsFree
msleep --> may sleep
isicom_set_termios
isicom_config_port
drop_dtr
WaitTillCardIsFree
msleep --> may sleep
isicom_tiocmset
drop_dtr
WaitTillCardIsFree
msleep --> may sleep
Though "in_atomic" is used to check atomic context,
but it is not recommended to use in driver code (see include/linux/preempt.h).
To fix it, only using mdelay instead.
This bug is found by my static analysis tool(DSAC) and checked by my code review.
Signed-off-by: Jia-Ju Bai <baijiaju1990@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
On most Renesas ARM platforms, the SCIF serial ports can be used with
DMA, so most users will want DMA support to be enabled.
On SuperH platforms, SCI(F) serial ports cannot be used with DMA yet
(see also commit 219fb0c143 ("serial: sh-sci: Remove the platform
data dma slave rx/tx channel IDs")), so users will want it disabled to
reduce kernel size.
Hence follow the above rationale to configure the default, unless
CONFIG_EXPERT is enabled.
Signed-off-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Renesas H8/300 and ARM platforms use DT and support earlycon, so most
users want earlycon support to be enabled.
On SuperH platforms, earlycon is not yet supported.
Hence follow the above rationale to configure the default, unless
CONFIG_EXPERT is enabled.
Signed-off-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Most users will want to use a serial console.
Hence make that the default, unless CONFIG_EXPERT is enabled.
Signed-off-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Auto-configure the maximum number of serial ports based on how many can
be present on the architecture:
- 3 on H8/300,
- 10 on SuperH,
- 18 on Reneas ARM.
The default can still be overridden if CONFIG_EXPERT is enabled.
Signed-off-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Using "make kvmconfig" results in a potentially unusable linux image
on s390. The reason is that both the (default on s390) sclp consoles
as well as the 8250 console register a ttyS<x> as console. Since there
will be no 8250 on s390 let's fence 8250. This will ensure that there
is always a working sclp console.
Reported-by: Alice Frosi <alice@linux.vnet.ibm.com>
Signed-off-by: Christian Borntraeger <borntraeger@de.ibm.com>
Reviewed-by: Hendrik Brueckner <brueckner@linux.vnet.ibm.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Invoke the ->rs485_config callback on probe to adjust the initial RTS
polarity based on the UART's device properties.
This implicitly fixes a bug: If RTS control is not available, rs485
should be disabled even if it was enabled through a device property.
Log an error when that occurs.
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Invoke the ->rs485_config callback on probe to set UARTMODEM_TXRTSPOL
appropriately based on the UART's device properties.
This implicitly sets UARTMODEM_TXRTSE if rs485 was enabled in the device
properties, so drop the identical code from lpuart_probe().
It also fixes a bug: If an unsupported rs485 property was specified
(rs485-rx-during-tx or rs485-rts-delay), the driver returns -ENOSYS
without performing any cleanup, in particular without calling
uart_remove_one_port() or clk_disable_unprepare(), thus leaking the
uart_port. But with the invocation of ->rs485_config, the unsupported
properties are now cleared in struct serial_rs485 and thus ignored.
It therefore seems sufficient to just log an error instead of bailing
out.
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When a driver invokes the uart_get_rs485_mode() helper, set the RTS
polarity to active high by default unless the newly introduced
"rs485-rts-active-low" property was specified.
imx contains a line to set the default RTS polarity to active high,
it is now superfluous and hence deleted.
omap-serial historically defaults to active low and supports an
"rs485-rts-active-high" property to inverse the polarity.
Retain that behavior for compatibility.
Cc: Mark Jackson <mpfj@newflow.co.uk>
Cc: Michał Oleszczyk <oleszczyk.m@gmail.com>
Cc: Rafael Gago Castano <rgc@hms.se>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit ef838a81dd ("serial: Add common rs485 device tree parsing
function") consolidated retrieval of rs485 OF properties in a common
helper function but did not #ifdef it to CONFIG_OF. The function is
therefore included on ACPI platforms as well even though it's not used.
On the other hand ACPI platforms with rs485 do exist (e.g. Siemens
IOT2040) and they may leverage _DSD to store rs485 properties. Likewise,
UART platform devices instantiated from an MFD should be able to specify
rs485 properties. In fact, the tty subsystem maintainer had asked for
a "generic" function during review of commit ef838a81dd:
https://marc.info/?l=linux-serial&m=150143441725194&w=4
Thus, instead of constraining the helper to OF platforms, make it
platform-agnostic by converting it to device_property_*() functions
and renaming it accordingly.
In imx.c, move the invocation of uart_get_rs485_mode() from
serial_imx_probe_dt() to serial_imx_probe() so that it also gets called
for non-OF devices.
In omap-serial.c, move its invocation further up within
serial_omap_probe_rs485() so that the RTS polarity can be overridden
with the driver-specific "rs485-rts-active-high" property once we
introduce a generic "rs485-rts-active-low" property.
Cc: Jan Kiszka <jan.kiszka@siemens.com>
Cc: Richard Genoud <richard.genoud@gmail.com>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Serdev currently does not support hangups so make sure to set CLOCAL to
prevent loss of carrier from triggering one.
Note however that not all tty drivers honour CLOCAL.
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Release the tty lock once tty-driver open returns to make it clear that
it does not protect neither tty->termios or the serport flags.
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Make sure to hold the tty lock as required when calling tty-driver
close() (e.g. to avoid racing with hangup()).
Note that the serport active flag is currently set under the lock at
controller open, but really isn't protected by it.
Fixes: cd6484e183 ("serdev: Introduce new bus for serial attached devices")
Signed-off-by: Johan Hovold <johan@kernel.org>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Make sure to use a properly refcounted tty_struct in write_wake up to
avoid dereferencing a NULL-pointer when a port is being hung up.
Fixes: bed35c6dfa ("serdev: add a tty port controller driver")
Cc: stable <stable@vger.kernel.org> # 4.11
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The receive_buf tty-port callback should return the number of bytes
accepted and must specifically never return a negative errno (or a value
larger than the buffer size) to the tty layer.
A serdev driver not providing a receive_buf callback would currently
cause the flush_to_ldisc() worker to spin in a tight loop when the tty
buffer pointers are incremented with -EINVAL (-22) after data has been
received.
A serdev driver occasionally returning a negative errno (or a too large
byte count) could cause information leaks or crashes when accessing
memory outside the tty buffers in consecutive callbacks.
Fixes: cd6484e183 ("serdev: Introduce new bus for serial attached devices")
Cc: stable <stable@vger.kernel.org> # 4.11
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If either uartclk or baud are 0, avoid calculating and setting a divisor
based on them since the output will almost certainly be garbage.
This also allows platforms such as the MIPS generic kernel, which has no
way to know a valid BASE_BASE for the board it is actually booted on at
compile time, to set BASE_BAUD to 0 and avoid early_8250 setting a bad
divisor.
This fixes a regression caused by commit 31cb9a8575 ("earlycon:
initialise baud field of earlycon device structure"), which changed the
behavior of of_setup_earlycon such that it sets a baud rate in the
earlycon structure where previously it was left as 0. All boards
supported by the MIPS generic kernel started outputting garbage from the
boot console due to an incorrect divisor being set.
Fixes: 31cb9a8575 ("earlycon: initialise baud field of earlycon device structure")
Cc: stable <stable@vger.kernel.org> # 4.14
Signed-off-by: Matt Redfearn <matt.redfearn@mips.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This device will be used in future Amazon EC2 instances as the primary
serial port (i.e., data sent to this port will be available via the
GetConsoleOuput [1] EC2 API).
[1] http://docs.aws.amazon.com/AWSEC2/latest/APIReference/API_GetConsoleOutput.html
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Matt Wilson <msw@amazon.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Since imx_disable_rx_int is only called by imx_startup,
let's integrate it into that function. Notice UCR2_ATEN is
never set by the driver. The bit is still cleaned to make
this patch a noop.
Signed-off-by: Troy Kisky <troy.kisky@boundarydevices.com>
Acked-by: Uwe Kleine-Koenig <u.kleine-koenig@pengutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit 075167ed71 ("drivers: PL011: replace UART_MIS reading with
_RIS & _IMSC") amended this driver's interrupt handler to read the
Raw Interrupt Status (RIS) and Interrupt Mask Set/Clear (IMSC) registers
instead of the Masked Interrupt Status (MIS) register. The change was
made to attain compatibility with SBSA UARTs which lack the MIS register.
However the IMSC register is cached by the driver. Using the cached
copy saves one register read per interrupt.
I've tested this change successfully on a BCM2837 (Raspberry Pi CM3).
Cc: Mathias Duckeck <m.duckeck@kunbus.de>
Cc: Phil Elwell <phil@raspberrypi.org>
Cc: Stefan Wahren <stefan.wahren@i2se.com>
Cc: Andre Przywara <andre.przywara@arm.com>
Cc: Mark Langsdorf <mlangsdo@redhat.com>
Cc: Naresh Bhat <nbhat@cavium.com>
Cc: Russell King <linux@armlinux.org.uk>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The mode constants are taken from the GPL-2.0+ driver available
in the driver section of the Moxa homepage.
It is tested on a C320Turbo PCI card per logic analyzer and
per a device which requires 9 bit character communication.
The vendors driver supports CMSPAR unconditionally, so that all
other available firmware versions seems to support mark/space
parity modes as well.
Signed-off-by: Lars Kanis <kanis@comcard.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
pl011_fifo_to_tty() has two counters (max_count and fifotaken) for the
same loop. One counter should suffice. This saves one subtraction per
character read from the RX FIFO.
Cc: Mathias Duckeck <m.duckeck@kunbus.de>
Cc: Phil Elwell <phil@raspberrypi.org>
Cc: Stefan Wahren <stefan.wahren@i2se.com>
Cc: Linus Walleij <linus.walleij@linaro.org>
Cc: Russell King <linux@armlinux.org.uk>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This simply fixes a typo in the preprocessor macros. No functional
changes intended.
Signed-off-by: Martin Blumenstingl <martin.blumenstingl@googlemail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In the code there are two separate sections which each describe some of
the bits in the AML_UART_CONTROL register.
Merge these into one section to make the code easier to read.
No functional changes intended.
Signed-off-by: Martin Blumenstingl <martin.blumenstingl@googlemail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The "clear error" bit in the AML_UART_CONTROL register is defined twice.
Remove the AML_UART_CLR_ERR definition and replace it with
AML_UART_CLEAR_ERR.
AML_UART_CLEAR_ERR was chosen to be kept since the datasheet's
description for this bit is "Clear Error" (so developer's don't have to
translate this to "CLR_ERR").
No functional changes intended.
Signed-off-by: Martin Blumenstingl <martin.blumenstingl@googlemail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Pointer gsm is assigned a value that is never read, hence it is
redundant and can be removed. Cleans up clang warning:
drivers/tty/n_gsm.c:2979:2: warning: Value stored to 'gsm' is never read
Signed-off-by: Colin Ian King <colin.king@canonical.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add code implementing managed version of serdev_device_open() for
serdev device drivers that "open" the device during driver's lifecycle
only once (e.g. opened in .probe() and closed in .remove()).
Cc: linux-kernel@vger.kernel.org
Cc: linux-serial@vger.kernel.org
Cc: Rob Herring <robh@kernel.org>
Cc: cphealy@gmail.com
Cc: Guenter Roeck <linux@roeck-us.net>
Cc: Lucas Stach <l.stach@pengutronix.de>
Cc: Nikita Yushchenko <nikita.yoush@cogentembedded.com>
Cc: Lee Jones <lee.jones@linaro.org>
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Cc: Pavel Machek <pavel@ucw.cz>
Cc: Andy Shevchenko <andy.shevchenko@gmail.com>
Cc: Johan Hovold <johan@kernel.org>
Cc: Sebastian Reichel <sebastian.reichel@collabora.co.uk>
Acked-by: Rob Herring <robh@kernel.org>
Reviewed-by: Sebastian Reichel <sebastian.reichel@collabora.co.uk>
Reviewed-by: Guenter Roeck <linux@roeck-us.net>
Signed-off-by: Andrey Smirnov <andrew.smirnov@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Using devres infrastructure it is possible to write a serdev driver
that doesn't have any code that needs to be called as a part of
.remove. Add code to make .remove optional.
Cc: linux-kernel@vger.kernel.org
Cc: linux-serial@vger.kernel.org
Cc: Rob Herring <robh@kernel.org>
Cc: cphealy@gmail.com
Cc: Guenter Roeck <linux@roeck-us.net>
Cc: Lucas Stach <l.stach@pengutronix.de>
Cc: Nikita Yushchenko <nikita.yoush@cogentembedded.com>
Cc: Lee Jones <lee.jones@linaro.org>
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Cc: Pavel Machek <pavel@ucw.cz>
Cc: Andy Shevchenko <andy.shevchenko@gmail.com>
Cc: Johan Hovold <johan@kernel.org>
Cc: Sebastian Reichel <sebastian.reichel@collabora.co.uk>
Acked-by: Rob Herring <robh@kernel.org>
Reviewed-by: Sebastian Reichel <sebastian.reichel@collabora.co.uk>
Reviewed-by: Guenter Roeck <linux@roeck-us.net>
Signed-off-by: Andrey Smirnov <andrew.smirnov@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Make use of the swap macro instead of _manually_ swapping values
and remove unnecessary variable tmp.
This makes the code easier to read and maintain.
This code was detected with the help of Coccinelle.
Signed-off-by: Gustavo A. R. Silva <garsilva@embeddedor.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
With all callbacks converted, and the timer callback prototype
switched over, the TIMER_FUNC_TYPE cast is no longer needed,
so remove it. Conversion was done with the following scripts:
perl -pi -e 's|\(TIMER_FUNC_TYPE\)||g' \
$(git grep TIMER_FUNC_TYPE | cut -d: -f1 | sort -u)
perl -pi -e 's|\(TIMER_DATA_TYPE\)||g' \
$(git grep TIMER_DATA_TYPE | cut -d: -f1 | sort -u)
The now unused macros are also dropped from include/linux/timer.h.
Signed-off-by: Kees Cook <keescook@chromium.org>
This changes all DEFINE_TIMER() callbacks to use a struct timer_list
pointer instead of unsigned long. Since the data argument has already been
removed, none of these callbacks are using their argument currently, so
this renames the argument to "unused".
Done using the following semantic patch:
@match_define_timer@
declarer name DEFINE_TIMER;
identifier _timer, _callback;
@@
DEFINE_TIMER(_timer, _callback);
@change_callback depends on match_define_timer@
identifier match_define_timer._callback;
type _origtype;
identifier _origarg;
@@
void
-_callback(_origtype _origarg)
+_callback(struct timer_list *unused)
{ ... }
Signed-off-by: Kees Cook <keescook@chromium.org>
Pull compat and uaccess updates from Al Viro:
- {get,put}_compat_sigset() series
- assorted compat ioctl stuff
- more set_fs() elimination
- a few more timespec64 conversions
- several removals of pointless access_ok() in places where it was
followed only by non-__ variants of primitives
* 'misc.compat' of git://git.kernel.org/pub/scm/linux/kernel/git/viro/vfs: (24 commits)
coredump: call do_unlinkat directly instead of sys_unlink
fs: expose do_unlinkat for built-in callers
ext4: take handling of EXT4_IOC_GROUP_ADD into a helper, get rid of set_fs()
ipmi: get rid of pointless access_ok()
pi433: sanitize ioctl
cxlflash: get rid of pointless access_ok()
mtdchar: get rid of pointless access_ok()
r128: switch compat ioctls to drm_ioctl_kernel()
selection: get rid of field-by-field copyin
VT_RESIZEX: get rid of field-by-field copyin
i2c compat ioctls: move to ->compat_ioctl()
sched_rr_get_interval(): move compat to native, get rid of set_fs()
mips: switch to {get,put}_compat_sigset()
sparc: switch to {get,put}_compat_sigset()
s390: switch to {get,put}_compat_sigset()
ppc: switch to {get,put}_compat_sigset()
parisc: switch to {get,put}_compat_sigset()
get_compat_sigset()
get rid of {get,put}_compat_itimerspec()
io_getevents: Use timespec64 to represent timeouts
...
Summary of modules changes for the 4.15 merge window:
- Treewide module_param_call() cleanup, fix up set/get function
prototype mismatches, from Kees Cook
- Minor code cleanups
Signed-off-by: Jessica Yu <jeyu@kernel.org>
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Merge tag 'modules-for-v4.15' of git://git.kernel.org/pub/scm/linux/kernel/git/jeyu/linux
Pull module updates from Jessica Yu:
"Summary of modules changes for the 4.15 merge window:
- treewide module_param_call() cleanup, fix up set/get function
prototype mismatches, from Kees Cook
- minor code cleanups"
* tag 'modules-for-v4.15' of git://git.kernel.org/pub/scm/linux/kernel/git/jeyu/linux:
module: Do not paper over type mismatches in module_param_call()
treewide: Fix function prototypes for module_param_call()
module: Prepare to convert all module_param_call() prototypes
kernel/module: Delete an error message for a failed memory allocation in add_module_usage()
These are the main MIPS changes for 4.15.
Fixes:
- ralink: Fix MT7620 PCI build issues (4.5)
- Disable cmpxchg64() and HAVE_VIRT_CPU_ACCOUNTING_GEN for 32-bit SMP
(4.1)
- Fix MIPS64 FP save/restore on 32-bit kernels (4.0)
- ptrace: Pick up ptrace/seccomp changed syscall numbers (3.19)
- ralink: Fix MT7628 pinmux (3.19)
- BCM47XX: Fix LED inversion on WRT54GSv1 (3.17)
- Fix n32 core dumping as o32 since regset support (3.13)
- ralink: Drop obsolete USB_ARCH_HAS_HCD select
Build system:
- Default to "generic" (multiplatform) system type instead of IP22
- Use generic little endian MIPS32 r2 configuration as default defconfig
instead of ip22_defconfig
FPU emulation:
- Fix exception generation for certain R6 FPU instructions
SMP:
- Allow __cpu_number_map to be larger than NR_CPUS for sparse CPU id
spaces
Miscellaneous:
- Add iomem resource for kernel bss section for kexec/kdump
- Atomics: Nudge writes on bit unlock
- DT files: Standardise "ok" -> "okay"
Platform support:
BMIPS:
- Enable HARDIRQS_SW_RESEND
Broadcom BCM63XX:
- Add clkdev lookup support
- Update clk driver, UART driver, DTs to handle named refclk from DTs
- Split apart various clocks to more closely match hardware
- Add ethernet clocks
Cavium Octeon:
- Remove usage of cvmx_wait() in favour of __delay()
ImgTec Pistachio:
- DT: Drop deprecated dwmmc num-slots property
Ingenic JZ4780:
- Add NFS root to Ci20 defconfig
- Add watchdog to Ci20 DT & defconfig, and allow building of watchdog
driver with this SoC
Generic (multiplatform):
- Migrate xilfpga (MIPSfpga) platform to the generic platform
Lantiq xway:
- Fix ASC0/ASC1 clocks
Minor cleanups:
- Define virt_to_pfn()
- Make thread_saved_pc static
- Simplify 32-bit sign extension in __read_64bit_c0_split()
- DMA: Use vma_pages() helper
- FPU emulation: Replace unsigned with unsigned int
- MM: Removed unused lastpfn
- Alchemy: Make clk_ops const
- Lasat: Use setup_timer() helper
- ralink: Use BIT() in MT7620 PCI driver
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Merge tag 'mips_4.15' of git://git.kernel.org/pub/scm/linux/kernel/git/jhogan/mips
Pull MIPS updates from James Hogan:
"These are the main MIPS changes for 4.15.
Fixes:
- ralink: Fix MT7620 PCI build issues (4.5)
- Disable cmpxchg64() and HAVE_VIRT_CPU_ACCOUNTING_GEN for 32-bit SMP
(4.1)
- Fix MIPS64 FP save/restore on 32-bit kernels (4.0)
- ptrace: Pick up ptrace/seccomp changed syscall numbers (3.19)
- ralink: Fix MT7628 pinmux (3.19)
- BCM47XX: Fix LED inversion on WRT54GSv1 (3.17)
- Fix n32 core dumping as o32 since regset support (3.13)
- ralink: Drop obsolete USB_ARCH_HAS_HCD select
Build system:
- Default to "generic" (multiplatform) system type instead of IP22
- Use generic little endian MIPS32 r2 configuration as default
defconfig instead of ip22_defconfig
FPU emulation:
- Fix exception generation for certain R6 FPU instructions
SMP:
- Allow __cpu_number_map to be larger than NR_CPUS for sparse CPU id
spaces
Miscellaneous:
- Add iomem resource for kernel bss section for kexec/kdump
- Atomics: Nudge writes on bit unlock
- DT files: Standardise "ok" -> "okay"
Minor cleanups:
- Define virt_to_pfn()
- Make thread_saved_pc static
- Simplify 32-bit sign extension in __read_64bit_c0_split()
- DMA: Use vma_pages() helper
- FPU emulation: Replace unsigned with unsigned int
- MM: Removed unused lastpfn
- Alchemy: Make clk_ops const
- Lasat: Use setup_timer() helper
- ralink: Use BIT() in MT7620 PCI driver
Platform support:
BMIPS:
- Enable HARDIRQS_SW_RESEND
Broadcom BCM63XX:
- Add clkdev lookup support
- Update clk driver, UART driver, DTs to handle named refclk from DTs
- Split apart various clocks to more closely match hardware
- Add ethernet clocks
Cavium Octeon:
- Remove usage of cvmx_wait() in favour of __delay()
ImgTec Pistachio:
- DT: Drop deprecated dwmmc num-slots property
Ingenic JZ4780:
- Add NFS root to Ci20 defconfig
- Add watchdog to Ci20 DT & defconfig, and allow building of watchdog
driver with this SoC
Generic (multiplatform):
- Migrate xilfpga (MIPSfpga) platform to the generic platform
Lantiq xway:
- Fix ASC0/ASC1 clocks"
* tag 'mips_4.15' of git://git.kernel.org/pub/scm/linux/kernel/git/jhogan/mips: (46 commits)
MIPS: Add iomem resource for kernel bss section.
MIPS: cmpxchg64() and HAVE_VIRT_CPU_ACCOUNTING_GEN don't work for 32-bit SMP
MIPS: BMIPS: Enable HARDIRQS_SW_RESEND
MIPS: pci: Make use of the BIT() macro inside the mt7620 driver
MIPS: pci: Remove KERN_WARN instance inside the mt7620 driver
MIPS: pci: Remove duplicate define in mt7620 driver
MIPS: ralink: Fix typo in mt7628 pinmux function
MIPS: ralink: Fix MT7628 pinmux
MIPS: Fix odd fp register warnings with MIPS64r2
watchdog: jz4780: Allow selection of jz4740-wdt driver
MIPS/ptrace: Update syscall nr on register changes
MIPS/ptrace: Pick up ptrace/seccomp changed syscalls
MIPS: Fix an n32 core file generation regset support regression
MIPS: Fix MIPS64 FP save/restore on 32-bit kernels
MIPS: page.h: Define virt_to_pfn()
MIPS: Xilfpga: Switch to using generic defconfigs
MIPS: generic: Add support for MIPSfpga
MIPS: Set defconfig target to a generic system for 32r2el
MIPS: Kconfig: Set default MIPS system type as generic
MIPS: DTS: Remove num-slots from Pistachio SoC
...
Here is the big tty/serial driver pull request for 4.15-rc1.
Lots of serial driver updates in here, some small vt cleanups, and a
raft of SPDX and license boilerplate cleanups, messing up the diffstat a
bit.
Nothing major, with no realy functional changes except better hardware
support for some platforms.
All of these have been in linux-next for a while with no reported
issues.
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Merge tag 'tty-4.15-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty
Pull tty/serial updates from Greg KH:
"Here is the big tty/serial driver pull request for 4.15-rc1.
Lots of serial driver updates in here, some small vt cleanups, and a
raft of SPDX and license boilerplate cleanups, messing up the diffstat
a bit.
Nothing major, with no realy functional changes except better hardware
support for some platforms.
All of these have been in linux-next for a while with no reported
issues"
* tag 'tty-4.15-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty: (110 commits)
tty: ehv_bytechan: fix spelling mistake
tty: serial: meson: allow baud-rates lower than 9600
serial: 8250_fintek: Fix crash with baud rate B0
serial: 8250_fintek: Disable delays for ports != 0
serial: 8250_fintek: Return -EINVAL on invalid configuration
tty: Remove redundant license text
tty: serdev: Remove redundant license text
tty: hvc: Remove redundant license text
tty: serial: Remove redundant license text
tty: add SPDX identifiers to all remaining files in drivers/tty/
tty: serial: jsm: remove redundant pointer ts
tty: serial: jsm: add space before the open parenthesis '('
tty: serial: jsm: fix coding style
tty: serial: jsm: delete space between function name and '('
tty: serial: jsm: add blank line after declarations
tty: serial: jsm: change the type of local variable
tty: serial: imx: remove dead code imx_dma_rxint
tty: serial: imx: disable ageing timer interrupt if dma in use
serial: 8250: fix potential deadlock in rs485-mode
serial: m32r_sio: Drop redundant .data assignment
...